Revisited... A few weeks ago my troubles came back. Same thing was happening. No reverse and no 2-3 upshift. Since last fall, I have watched many utube videos on the 4r100. I know enough to be really dangerous now.
![Roll Eyes ::)](http://fepower.net/simplemachinesforum/Smileys/default/rolleyes.gif)
So I pulled the pan, main valve body and modulating body. I was looking for the 2-3 valve to be stuck in the main VB. But all was ok. The mod body did have a stuck valve tho. This was not what I wanted to find. Everthing I had read and seen told me the mod body would not cause the problem I was having. I hauled my bodies down to a reputable local tranny guy for a show and tell. What he said was encouraging. Depending on the year of the seperator plate, a stuck valve in the mod body can cause my problems. So with this advice, I liked my odds again. I bought the Accutech mod body for the Powerstroke and put everything back together. Filled it with cheap oil. (just in case the whole thing needed to come out) And crossed my fingers. And how about that....IT WORKS! IT WORKS! What a different animal now also. The shifts are short and crisp. But not hammering, like when I was running the hot program from the Hypertech tuner.
So today, I took the banjo bolt out on the pressure side cooler line and tig welded the holes so oil won't bypass to the return side without circulating to the cooler first. (more utube wisdom) Also installed an external Balwin filter and shelled out for full synthetic oil.
Next with be a tranny temp guage. And a very light foot.......
![Grin ;D](http://fepower.net/simplemachinesforum/Smileys/default/grin.gif)