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Topics - jayb

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17
FE Technical Forum / FE Power at the FE Race and Reunion
« on: September 05, 2021, 10:58:27 AM »
We will be at the event, showcasing the first production cylinder heads and related items, plus of our standard products.  If you will be attending the show and want to purchase any FE Power items, please leave a response here, or message me, or email me (jayb@fepower.net), or give me a call (952-428-9035), and I will bring the product you want to the show, to save you some shipping expense.  FYI, we are still out of intake adapters, but have limited numbers of timing covers and timing sets available.  We will also be running a show special on books.  Looking forward to seeing all my FE friends at the Reunion!

18
Private Classifieds / Wanted - Passenger Side 428CJ Exhaust Manifold
« on: September 01, 2021, 10:25:16 AM »
A friend of mine is looking for one of these.  If you have one, or have a set you want to sell for a reasonable price, please let me know.  Thanks, Jay

19
Vendor Classifieds / The Great FE Intake Comparo is back in stock!
« on: August 11, 2021, 04:27:29 PM »
After nearly a 6 month delay, I finally received my next printing of books yesterday.  They are available now for immediate shipment.  If you are one of those folks who paid for a book and is now waiting for it, it shipped out earlier today (8/11/21), and thanks so much for your patience - Jay

http://www.fepower.net/GFEIC.html

20
FE Technical Forum / What the heck is going on in the oil pan?
« on: August 05, 2021, 04:22:59 PM »
I've been doing a little more testing on the dyno mule with my cylinder heads on it this week (up to 894 HP now).  After the last go around a few weeks ago I had some conversations with a couple of my head customers, and John S (oldiron.fe on the forum) mentioned putting a window in the oil pan to see what was happening.  Ever since I started with this engine on the dyno last September, I've noticed that at the higher RPM pulls I have a significant decrease in oil pressure, typically starting around 65 psi at 5000 RPM and dropping to about 50 psi at 7000 RPM, with the oil temperature around 180 degrees, using 10W-30 VR1 Valvoline oil.  Higher oil temps of around 200 degrees make it a few psi lower, and I really wasn't too comfortable with those levels.  I've seen this oil pressure issue before with vacuum pumps, so I figured that was a contributing factor, but I thought it would be interesting to see exactly what the oil in the pan was doing.

Since I was planning on pulling the pan to check the bearings, I decided to go ahead with the window, potentially wrecking the oil pan but hopefully learning a few things in the process.  After checking all the bearings (which looked almost new), I cut a big rectangular window out of the Milodon 7 quart oil pan and bolted a piece of 3/8" thick clear polycarbonate to the side, using a bunch of The Right Stuff to seal it.  The engine is using a Moroso windage tray between the block and the pan, and a Precision Oil Pumps high volume pump using the small spacer between the spring and the cup plug.  I've also installed a new vacuum pump from Star Machine to replace the GZ Motorsports pump that I had been running previously.  This pump gave me a few more inches of vacuum, and probably contributed to the latest HP numbers.

I set up a camera to take videos of the window in the oil pan while the engine was running, and during a dyno pull.  I also rigged up a tach so that you could see the engine speed in the video, but unfortunately the tach I used didn't work, or else it didn't like the tach signal from the MS3-Pro.  Regardless, I started testing the engine and then watching the videos.  I was really surprised at what I saw.  The first video link is below; this is with a total of 8 quarts of oil in the engine.  It takes a while in the video to get to the actual dyno pull, which happens starting around 1 minute and 45 seconds in.  The oil levels are marked on the pan in the video:

https://youtu.be/ZPL_05cKRKY


Wow, the amount of air entrained in the oil during the actual dyno pull is shocking!  Lots of big bubbles circulating in the oil, certainly contributing to aeration of the oil coming out of the pump.  As my dyno junkie friend Royce said, it looks like you are spraying a garden hose into a bucket of water.  There appears to be about 6 quarts of oil in the pan during idle, and it drops to about 4 quarts during the pull.  A while back on the Engine Masters show on Motor Trend on Demand, they did an experiment where they saw oil pressure drop as engine speed increased, attributed it to foaming of the oil, and solved the problem by taking some oil out of the pan.  I thought I would try the same thing, so we pulled 2 quarts out of the pan, and ran the test again.  Here is the video:

https://youtu.be/cQRGg-nI8m0


Well, that didn't work, we still had the same drop in oil pressure as before up at 7000 RPM, we seemed to have the same amount, or even a bit more, of foaming and bubbles in the oil, and we didn't make any extra power.  The oil level in the pan looked like 4-1/2 quarts during idle, and about 3 quarts at peak RPM. 

The obvious next test was to remove the vacuum pump and see how it looked without the pump on the engine.  We went back to 8 quarts of oil in the engine, and ran without the vacuum pump.  Here is the video:

https://youtu.be/sd29Ye2E0Q4


Unfortunately for this video I had decided to remove the tach (which wasn't working), and apparently after repositioning, the camera position was off a little compared to the last two videos, and we got some glare from the window that kind of obscured the oil.  However, if you look closely you can see that the oil level in the pan drops quite a bit farther in this video than in the first one, and there still seems to be a whole bunch of foaming and air bubbles in the oil.  BUT, the oil pressure stayed stable throughout the dyno pull.  Unfortunately the oil pressure win was offset by a large HP loss.

Based on the fact that the engine has been behaving like this (oil pressure wise) for several dyno sessions, and that the bearings looked very good when I inspected them, I'm not overly concerned about the oil pressure issue when the vacuum pump is running.  However, it seems like there ought to be some oiling system modifications that could mitigate this problem.  One thing I tried with this new vacuum pump setup was a second vacuum port lower in the engine; this was recommended by Star Machine, and also Andy Miller at Olds Performance.  I actually put a hole through the side of the block right across from the #3 main cap, and then milled a slot in the main cap to allow air from the crankcase into the slot, through the hole, and out to the vacuum pump.  The hope was that since the hole in the block was shielded by the cap, it wouldn't draw in too much oil, but that didn't work, so I went back to a single line from the valve cover to the vacuum pump.  I might try that again next time around with a baffle over the slot in the cap; Lykins also suggested going through the fuel pump opening in the timing cover, so I could try that too.

Another thing is the windage tray.  The Moroso tray has louvers that strip oil off the crank, and several of those louvers point straight down at the oil level in the pan.  You can see this in the videos when the engine is idling, one of those louvers is right above the window and oil is coming straight down.  It seems like using the Ford windage tray, which has louvers only on the right side of the engine and shoots the oil horizontally through the louvers, rather than vertically, would be a better design.  Also it seems like a kickout on the right side of the oil pan, designed to catch that oil and give it a chance to slow down before it hits the rest of the oil in the pan, would be good.  It's also possible that a screen on the windage tray, like the Canton pan has, would lead to less foaming in the oil.  Maybe no windage tray at all would work best? 

Maybe the standard volume pump would yield an improvement.  And of course if you ran a really, really deep pan, that also might help.  The list goes on...

I'm sure there will be a million theories on the best approach to this issue, but the problem is there is very little data to back up the theories, and getting data requires changing up oil pans, windage trays, oil pumps, etc., which of course is a huge pain.    But if I go forward with any modifications I will certainly post them here for general interest.  I'm not sure if there is really HP to be had with a better oil pan setup, but an improvement in the stability of the oil pressure would be a worthwhile goal.

21
FE Technical Forum / Installing an FE main stud girdle
« on: July 23, 2021, 02:29:35 PM »
On my 390 stroker project in the Member Projects section I had been looking to use a main stud girdle, but couldn't find one available at the time I wanted to do it, so I went with crossbolted main caps instead.  They were expensive, and a real pain to install.  I wanted to try installing a girdle as a comparison, and it turned out that one of my cylinder head customers was going to use a 390 block and put a girdle on it.  I offered to install it for him at no cost because I wanted to see how difficult it would be.  He was able to find a girdle like the one I wanted to use, so last week he drove up to my place and dropped off the block and the girdle and hardware.  This week during a break in the action I got his block on the CNC machine and started the installation.

My plan was to precisely indicate the height location of the five main cap registers in the block, then shim up the block to make them as level as possible.  From there I wanted to cut a few thousandths off the pan rail, in order to make sure that it was square with the main cap registers before machining the caps and bolting on the girdle.  I had been told that the oil pan rail would not necessarily be square with the main cap registers, and in order to make the girdle a nice fit I wanted to make sure that it was.

By the way, the directions that came with the girdle didn't suggest anything like this, basically saying to use the oil pan rail as it was.  This didn't sound right to me, since if the pan rail turned out not to be square with the main cap registers the girdle would have to deform to fit. 

Anyway, I set the block up on the CNC table, resting with the main cap registers facing up and roughly aligned square with the table, clamped it in place, and started measuring the height of the main cap registers.  This was done with an arbitrary Z axis setting; all I was interested in was how the main register heights compared with each other.  I figured that they would all be very close, and I was surprised at how close they actually were.  On the right side of the block, they were all within 0.002" of each other, and the left side was only a little worse:




On average the left side of the block looked just a couple thousandths higher than the right side of the block, which I thought was pretty good given that the block was sitting upside down, and relying on the squareness of the end rails relative to the main cap registers.  In order to make the main cap registers as level as possible, I used some .004" shim stock under the right side of the block's end rails on each end.  I remeasured and got the following results:




This brought the height of the #2 and #3 main cap registers just about the same, and #4 was only off by a thousandth.  #5 was off by almost 0.005", but that wasn't a concern because the girdle doesn't tie into the  #5 main cap.  The left side of #1 was about 0.004" higher than the right side, and I figured I could compensate for that with the spacers.

Now that the main registers were as squared up as I could make them, I measured the height of the oil pan rail in the four corners of the block:




These results were not nearly as bad as I had been led to believe; worst case variation was only about 0.010", and since the distances across the block were much greater than the distances across the main cap registers, it really wasn't that bad.  Nevertheless, I set up my 3" facing mill and took about 0.012" off the oil pan rail, to square it up with the main cap registers:




This whole process, from getting the block fixtured on the CNC machine, to cutting the pain rail, took about an hour and half.  No big deal.

Next I took caps 1 through 4 and put them into the vise on my smaller CNC machine.  I indicated off the ways of the vise in the Z axis, and then indicated on each main cap bolt hole to find it's center.  Then I wrote a short CNC program to spot face the bolt holes in the top of the caps, to make them all exactly the same height.  I tried to go to a 2.5" height from the bottom of the caps up to the spot face, but it turned out that one of the caps was a little lower than that, so I went down to a height of 2.475" to get all the spot faces on the caps exactly the same height from the bottom of the caps.  It took about an hour to machine the caps.

Another quick aside is that the manufacturer provides a spacer between the cap and the girdle that is a single piece strap for each cap, with two holes in it.  They tell you to bolt the girdle on the block, then measure the distance from the main cap registers up to the girdle, subtract the thickness of the strap, and machine the whole top of the cap to get the height to that dimension.  I also did not like this idea, it seemed to me that getting a precise measurement of this distance would be problematic, and also machining any more off the cap than necessary would limit the strength of the cap.  So I elected not to use the straps, and decided to make up some donut spacers instead.

With the block still fixtured on the CNC machine, I measured the distance between the main cap registers and the oil pan rail, subtracted the 2.475" distance from the cap base to the spot face, and found that I needed spacers about 0.182" thick.  Due to slight variations in the height of the registers, I ended up machining spacers of slightly different thicknesses, ranging from 0.180" to 0.184".  This was the most time consuming part of the project, and hindsight being 20/20, I can think of a much easier way to do this; more on that shortly.  It took me about 3 hours to get these 8 donut spacers machined:




From there I assembled the main studs in the block.  The stud kit included two studs that were shorter than the other eight, for use in the #5 cap, but actually they were still too long to be used, and even with the presence of the girdle they would stick up above the oil pan rail.  The instructions said they "may" need to be cut to fit  ::)  Anyway, I had known about this issue and had the block owner buy some special, shorter studs for the #5 cap.  To make the stud washers and nuts fit, I also counterbored the #5 cap 0.275".  I installed the studs, the caps, and the spacers in the correct location to make them all the same height, then finally I installed the oil pan studs that came with the kit; here's a picture of how the block looked at this point:




The girdle fit nicely down on the block, and in fact it could be wiggled around a little; probably the holes for the studs are slightly oversize.  The main stud washers and nuts were installed next.  The kit comes with some thin nuts that fit into the counterbored areas of the girdle.  I found that the counterbored holes were too small for my 3/8 drive 1/2" socket to fit, so I couldn't use that to tighten the nuts; I ended up going to a 1/4 drive ratchet and socket to get them tight. 




The last thing I did was to machine a couple of precision holes for some 3/8" diameter steel pins, in order to positively fixture the girdle on the pain rail.  I was uncomfortable with the fact that the girdle could slide around some when it was placed over the studs, and despite being clamped down, I wanted a more positive location for it.  So I machined two holes through the girdle and into the block, and will install some steel pins to lock it into a fixed position.  Here's a photo of one of the holes:




Having installed one of these now, I can say by comparison it is a much easier installation than the cross bolted caps.  With the crossbolted caps, the block has to be perfectly aligned in the X axis of the mill, and also perfectly machined to make the caps fit properly.  Then, the block has to be set up on the machine rotated 90 degrees along the X axis to drill the holes for the cross bolts on one side, then it has to be set up at -90 degrees to drill the crossbolt holes on the other side.  This is a ton of setup work, and horsing the block around to these different positions, and then fixturing it in those positions, is very time consuming.  Not to mention tapping the cross bolt holes in the caps.

Despite being more expensive by around $200, and requiring much more expensive machine work, the cross bolted caps are probably more rigid than the standard caps using a girdle.  My take on this though is that given the cylinder wall and main web thickness of a 390, the cross bolted caps may be overkill.  I'm pretty sure that the girdle will make the block able to withstand 650-700 HP, and it probably wouldn't be a good idea to go beyond that with a 390 block anyway.

One issue with the girdle that I don't like is that the spacers have to be kept in the same position, in order to maintain minimum stress on the girdle.  Since they are slightly different thicknesses, if you mix them up you may impart a twist into the girdle when it is assembled.  I thought I was going to be able to address this by just stamping or scribing each spacer with it's position, but that didn't turn out to be practical; the steel was not easy to scribe, and when I tested stamping an extra spacer, it raised the material around the stamp mark and changed the thickness.  So the spacers need to be carefully marked when removed, and then replaced in the same spot.

Another concern with the girdle is that if you want to run a windage tray, it is going to be spaced 3/8" farther from the crank, making it a little less effective.

Speaking of the spacers, if I was going to do this project again, I'd take advantage of the precise ring shims available from McMaster Carr.  For example, they have a 0.188" thick spacer with a thickness tolerance of +/- 0.007", and they have .001" and .002" thick ring spacers, with thickness tolerances of much less than .001".  Having a selection of those on hand, and cutting the main cap spot faces just a little deeper than I did, would allow these off the shelf shims to be used as the spacers, taking the majority of time out of this project.  If I ever do another one of these, that's what I'll do.

One last comment is that after this work is done, the block should be align honed, if it hasn't been already.  Sometimes the machine shop will take a few thousandths off the bottom of the caps to align hone the main saddle.  If that happens, then some of those really small shims mentioned previously will have to be added to the shims that are already in place between the girdle and the caps.  For example, if the shop takes .002" off the bottom of each cap, then a 0.002" shim should be installed with each spacer.  But again, since those shims are readily available, no big deal.

I hope this quick tutorial will help if you are considering a girdle for your engine.  Anybody with a vertical mill can do this work, although it is a little easier with CNC, and it seems like a good upgrade for a 390 or 428 block that is headed for serious horsepower.

23
FE Technical Forum / More FE Power Cylinder Head Dyno Results
« on: July 10, 2021, 10:17:27 AM »
It's been mid winter since I've run the dyno mule with my cylinder heads, and despite having several tests that I've needed to run, work on getting the head package into production has taken a bunch of time so I didn't get back at the dyno testing until this week.  All along my friend Royce B has been mercilessly hounding me to get back on the dyno LOL!  Royce is a dyno junkie, and wanted to come up to help.  Finally on Wednesday this week my schedule opened up, Royce arrived and we got going again with the testing.

It had been quite a while since the last test, so the first order of business was to baseline the dyno mule again.  The unported SE cylinder heads and the 8V intake with two Dominator carbs were on the engine, and the cam was still the same cam Brent Lykins got for me last winter.  Previous best was 861 HP with this combination.  After debugging an electrical problem we got the engine running correctly, and I was happy to see some even better results; the engine peaked at 869 HP and 730 lb-ft of torque. 



Later during the analysis I discovered that I had left the RE timing spec in the EFI software, which was 30 degrees total instead of 28 degrees total as I had originally run with the SE heads.  So that little tweak to the timing probably explains the slight improvement.  Nevertheless, we were back to baseline and ready for more testing.

Over the last several months I've been designing some new intake manifolds to use with my heads.  I'm actually quite happy with the performance of the 4V intake, but the 8V intake isn't working as well as I'd hoped.  I tried to design the 8V intake as something similar to the tunnel wedge for use with my heads, but in the quest for power I kept the runners straight, and it ended up not looking like a tunnel wedge manifold at all, and not having the plenum volume and design of a modern sheet metal style intake either.  So I went back to the drawing board and the 3D printer, and ended up designing two more 8V intakes in the more traditional sheet metal style.  Also, in speaking with a few of my cylinder head customers, some of them had hood clearance concerns, so I elected to do an 8V intake design that was lower, and did look like a traditional tunnel wedge manifold.  Finally, I also wanted to do a lower 4V intake, and after making some measurements I concluded that using a low profile EFI throttle body, I could actually make the intake work with a shaker or ram air setup.

My 3D printer has been balky over the last few months, and I've had to make some repairs and part replacements to keep it running properly, but after a few false starts I finally got all four of these intakes printed.  This is the low version of the 4V intake, sitting on an intake adapter:




The photo below is the low version of the 8V intake, designed in the tunnel wedge style:




This one is one version of a sheet metal style intake, with short runners and a lot of taper:




This is the other version of a sheet metal style intake; this one has longer runners and less taper, and is shown mounted on the engine:




I've been thinking about running these plastic manifolds on the dyno for a while, and one concern was if they were going to be airtight or not.  Before the dyno session I had briefly considered painting them all to try to make sure that the external surfaces were all leak free, but I didn't get around to that before the dyno session, so I decided to just bolt on the red sheet metal style manifold and try to run it.  Unfortunately, when we started the engine it was obvious that there was a big vacuum leak, and a few seconds after starting the engine, it backfired and broke the plastic manifold.  So, it was clear that some sort of sealing on the external surfaces of the 3D printed intakes was going to be required.  The joys of R&D...

At that point we decided to swap over to the RE heads.  We had not yet tested the RE heads with the Lykins cam, and since that cam had picked up the engine with the SE heads substantially, I was anxious to see how it would improve the performance with the RE heads.  Pretty much all day Thursday was devoted to the swap, since in addition to just changing the heads, all the valves and springs had to be swapped from the SE heads to the RE heads also.  We finally got the engine all back together with the 8V intake at the end of the day on Thursday, and started it up to make sure that everything was OK.  The engine sounded good, so we were primed for a good dyno session on Friday.

Friday's dyno session did not disappoint.  After a couple of checkout pulls, we ran the engine to 7000 RPM, and much to my surprise, it appeared to be still climbing in power at that point.  I really didn't want to run past 7000 with the RPM crank that is in the engine, but we decided to make a 5300-7300 RPM pull and see what happened.  We were rewarded with just over 881 HP, and again the engine still appeared to be climbing at 7300 RPM:




Next step would have been running to 7500 RPM, but as the engine came out of the pull on the previous run, Royce and I thought there may have been some valvetrain noise.  So out of an abundance of caution we decided to pull the valve covers and check the lash.  Sure enough, the #6 exhaust lash had increased from .016" to .030", and that was probably what we had been hearing.  We immediately suspected a lifter was going away; the Crower roller lifters I've had in this dyno mule have been around for a while and used in different engines, and we've had to replace a few of them during the course of this testing.  So, reluctantly we pulled the intake and carbs, and opened up the plate in the middle of the intake adapter so we could pull the #6 lifter.  However, checking it there were no obvious problems.  Next I disassembled the rocker arm pair from #6, and again everything looked fine.  I don't have an explanation for the increased lash, unless I just didn't tighten the adjuster enough when I set it.

At this point we decided to just go to the 4V intake, since we were happy with the results of the 8V.  We installed the 1150 Dominator carb on the intake, and ran again.  Previous best with the old cam had been 857 HP, but the new cam bumped us up to 873 HP, and also a bit of a torque increase:




One thing about the 4V intake was that it did not appear to be making power all the way to 7000 RPM.  In fact we ran two pulls to 7300 RPM, and in both cases the power did not increase, and in fact the engine seemed to miss a little past 7000 RPM.  A look at the air inlet data gave a clue on this, as the engine was requiring very close to the 1150 cfm of air that the carb was rated for.  We saw vacuum levels of as high as 1.6 inches with the 4V intake and carb, where vacuum levels for the 8V setup were zero through the whole RPM range.  So obviously the engine liked the 8V setup better.

Thursday I had taken the time to paint the exterior of the remaining 3D printed intakes, to try to seal them up.  The 8V tunnel wedge intake also had some gaps in the plastic that the paint wouldn't fill, so Royce took a caulk tube of The Right Stuff and attempted to seal up those holes.  By the time he was done, he had slathered about 2/3 of the intake with that stuff LOL!  It was ugly, but we hoped it would seal.  We decided to do that intake next, so Friday afternoon we bolted it on the engine with two 660 center squirter carbs, and tried to run.  But again, it was obvious that there was still a vacuum leak; the engine would burn through the pump shot and then die.  We didn't want to risk breaking that intake with a backfire, so we stopped the testing. 

As a final experiment with the plastic intakes, we took the low 4V intake and sealed up the carb pad with a plate, then taped off the runners on one side and filled the intake up with water.  We were very surprised that despite being painted to seal it up, it was still leaking like a sieve.  We had water dripping out of the bolt holes, the bottom of the plenum area, and some of the runners.  So obviously just painting the intake with Rustoleum was not going to get it sealed.  This week I'm going to be working on a better sealing procedure for the 3D printed intakes, and also a test rig so that I can test them for leakage with a few psi of air, prior to actually installing and running them on the engine.  I'm sure that they can be run if I can fix the sealing issue, and it will be good data to have before deciding if I want to proceed in production with them or not.

Regardless of those issues, I'm very pleased with the power numbers from the existing 4V and 8V intakes.  I'm close enough to 900 HP now that with some tweaks I'm sure I can reach that goal with this engine, which I think is pretty cool with heads where the ports are still rough cast.  I'm not running much crankcase vacuum, only about 7", so I may increase that somewhat to pick up some power.  Lykins thinks I should run some shear plates under the carbs, so I may try that.  I may also try a bigger primary tube on the headers; I picked up substantial power going from 2" to 2-1/8", so it may be worth building a set of 2-1/4" headers just to test on the RE heads.  When I have more data I will put it up here; I'm particularly looking forward to running the single piece crossram intake, which is ready to be cast as soon as the foundry can open up a slot to pour it.  Stay tuned...

26
Member Projects / 390 Stroker for FE Power Cylinder Heads
« on: June 24, 2021, 04:57:12 PM »
One of the things I've wanted to do with my cylinder head package is to put it on a fairly standard 390 stroker engine, and see how it performed.  I've had a little break in the action on the head project, because the aluminum foundry is really backed up and despite ordering castings for the intake adapters and heads in March and April, they have still not been poured, so I decided to get a head start on this project.  I have two 390 blocks here that I could choose from, so I decided to sonic test them and pick the best one.

One of the blocks is already .040" over; this is the block that was the basis of my 390 stroker engine, featured in my book.  I had set this engine on the stand and forgotten about it for the last 10 years, so a few days ago I pulled it all apart so I could check it.  Everything looked very good, which was encouraging after all the dyno abuse that this block saw.  But when I sonic tested it, there were a few holes that looked a little thin to me.  The sonic test results are below:



In particular, the front side of cylinders 2 through 4, and the back side of cylinders 6 and 7, looked a little thin.  I was going to bore this block another .020", and my arbitrary requirements for minimum cylinder wall thickness is 0.100" after boring for non-thrust surfaces, and 0.125" after boring for thrust surfaces, hopefully with more thickness on the major thrust side (shown in red in the picture) than on the minor thrust side (shown in yellow).  Several cylinders on this block weren't going to meet these requirements.  Now, of course this block took a bunch of abuse at 500+ HP on my dyno, and as-is cylinder 4 is below my requirements, and there weren't any problems, so maybe I shouldn't be too concerned.  But I decided to check the other block out and see if it looked better.

Turned out it did; the sonic check data for that block is below:



This block is currently standard bore, which helps of course, and the areas of concern were the minor thrust sides on cylinders 5, 6, and 7.  Again I was figuring to bore this block .020" (0.010" on each side), and I'd be below my arbitrary requirements on the minor thrust side of these cylinders.  However, I'm a big believer in sleeves, since they are actually better material than the block material itself, so I think I will sleeve 5 and 7, and leave 6 as-is, to make this block as robust as possible. 

Since I was going to abuse this engine somewhat, I had previously decided to run a girdle.  I had never used one and wanted to try one out, and there had been one appearing on ebay that I thought looked pretty good.  I was planning to pin the rail of the girdle to the pan rail, so that it couldn't move, and then machine some precision spacers to go between the girdle and the main caps.  I was going to bolt it all together, take the block in for an align-hone, and then if the caps had to be cut a few thousandths, compensate with some shim stock between the caps and the girdle.

This approach went out the window though, when I went back on ebay and the girdle I was looking at was no longer listed.  However, there was a set of Pro Gram caps listed.  Well, that was going to be a much bigger machining project to make them fit, but I didn't want to wait for the girdle because I have some time now, and won't have it later.  So, I went ahead and bought the set of Pro Gram caps.  I also purchased an ARP main stud kit to use with the caps.  Pictures of the parts are below:




So right off the bat I have more into this project (about $500) than I would have had with the girdle, and I had some serious machine work on the block to do.  When the parts arrived the stud kit looked fine, but unfortunately the cross bolts and washers were not included with the caps, as they should have been.  I contacted the seller and they are supposedly on the way to me now, but to get going on this project I dug up some grade 8 bolts that I could use for the crossbolts.

The instructions that came with the caps tell you how to machine the block to make them fit.  One thing I found a little strange was that the instructions were from a company called Billet Speedworks; no mention of Pro Gram Engineering anywhere.  Nevertheless, I hoisted the block up onto my big CNC machine, and cut the sides for clearance to the ears of the caps.  The first picture below shows the block on the machine, and the second picture shows one side of the block after the machining operation is complete:






One thing I found helpful is the location of the two holes on the right side of the FE block, as shown in the photo above.  These holes are used to bolt the block to the cradle during Ford's assembly operation and were in the perfect spot to line up with the ears of the caps once they were installed.  I was able to install the caps temporarily at this point (see the picture below), and then use those holes to mark the caps for the crossbolt locations on two of the caps.  This also gave me a reference to the pan rail, so that I could transfer the dimensions to the middle cap, and the left side of the block.



After marking the caps, I transferred them to the smaller CNC machine.  I measured the two marks that I'd made with the caps installed and duplicated those hole positions on all three caps, both ends.  Then I drilled and tapped the ends for 3/8-16 thread.  I also drilled and tapped a 5/16-18 hole in the center of each cap, because I found them difficult to remove from the block after the first test install.  With the tapped hole, a slide hammer can be used to remove them, similar to what is required with some of the aftermarket blocks.  A picture of the caps after the last machining operation is shown below:




While I was at it, I also pulled the stock #5 main cap out and counterbored it 0.275", to allow the nuts for the ARP studs to sit below the pan rail.  I was happy to see that the two studs for the rear cap were shorter, so the studs themselves didn't extend up beyond the pan rail, but left as is the nuts and washers would have.  Counterboring the cap was pretty easy, compared to all the other machining operations I had to do for this project.

I was hoping that I'd be able to drill the holes in the block for the crossbolts without having to put the block back on the CNC, but that didn't work out.  I tried to do it with my drill press but the travel of the drill press didn't reach all the way down to the block, as it was sitting on the engine stand.  I also tried a hand drill, using a 1-2-3 block as a fixture to ensure that the hole went in square with the side of the block, but I couldn't easily get a clean hole; the drill tended to drift around too much.  So, in the end I gave up and put the block back on the CNC machine to drill and spot face the cross bolt holes, as shown in the photo below:




After flipping the block over to get to the holes on the other side, finally I was able to pull the block off the machine and install the caps and crossbolts:




And of course, I'm not done yet, because the caps are undersized, and so now the block has to be align bored and then align honed in order to get the bearing clearances right.  Depending on how much that costs, I think I'll probably have between $800 and $900 in this project, plus all the machine work I did myself.

Anyone with a Bridgeport or other vertical mill could do what I did to this block, but it is a painstaking operation and takes quite a bit of time; I think I had 8-9 hours in the whole project.  If you have to pay to get the machine work done that I did, seems like you'd be better off just getting an aftermarket 427 block.  I think adding a girdle would be much easier and cheaper, and next time I do something like this that will be my preferred approach.  But for now, I think I've got a block that I'm comfortable with up to the 700 HP level.  I'll add more information to this post as the engine goes together, but it will be a while; pistons are 8-10 weeks out...

27
FE Technical Forum / Just Another Day in the Life of a Car Guy...
« on: May 04, 2021, 05:30:31 PM »
Quite a few years ago David Freiburger wrote one of his back page columns for Hot Rod entitled, "Life at the Side of the Road".  It talked about the inevitable breakdowns that all of us suffer with our high performance equipment.  It struck a chord with me because I'd been there, probably like most of us on this forum.  I was there again yesterday  :D

I was on my way to my friend Steve's house to see his progress on my 69 Torino; Steve is doing the bodywork.  Three quarters of the way there in my 68 Mustang with 428CJ, I stopped at a stop light and heard a noticeable ticking sound.  Hmmm, did I just develop a header leak?  I turned the corner and accelerated and suddenly things got dramatically worse; the engine was backfiring and popping, the car bucking and lurching, etc.  Oil pressure was down to about 20 pounds, from a normal 60.  I pulled into the nearest parking lot just as it died, wondering what the heck had gone wrong.

I popped the hood and through my trick FE Power clear valve covers ( ;D) I could see that the #4 exhaust rocker had broken.  This was a Comp Cams rocker, one of the extruded aluminum ones that Dove used to make for Comp.  They are known to fatigue and fail after a while, but I hadn't been too worried about this because the valve springs on this engine are pretty mild.  Apparently that didn't matter to this particular rocker arm.  The engine has been together since 2008, and I put a couple thousand miles a year on it, so I guess it doesn't owe me anything, but still...

Anyway, with just a busted rocker I figured I could limp the remaining 3-4 miles to Steve's place.  I got the engine started and found sort of a sweet spot where the engine would run without a whole bunch of drama, and pulled into Steve's driveway.  At least I wasn't on the side of the road LOL!  I had a spare rocker arm at home, so I borrowed Steve's truck to get back there, and while I was gone he pulled the valve cover.  When I got back he had the offending rocker out, picture below:




Nice!  While I had been at home I called Steve and had him check the pushrod, and it was still straight, so I figured we'd just pop in the new rocker and I'd be ready to go.  Unfortunately, when we got ready to reinstall the rocker assembly with the new rocker, we discovered that the lifter had come completely out of the bore, and was laying in the valley.  No wonder the oil pressure had gone away.  At the rear of the engine compartment, the hood hinge and spring were in the way of really seeing anything, and it was clear that we weren't going to be able to fish that lifter around through the holes in the intake and get it back in the bore.  It was getting dark, and I didn't want to impose any further, so Steve lent me his truck and I went home, figuring I'd fix the problem today while he was at work.

I got over there early this afternoon after taking care of some FE Power stuff in the morning.  My plan was to leverage the features of the FE Intake Adapter to open up the valley of the engine, reinstall the lifter, and button everything back up.  Everything went fine at first; I had the intake and carb off in 15 minutes, and the center plate of the intake adapter off a couple minutes after that.  There was the lifter just laying there in the valley, so I stuck it back in the bore.  However, quite unexpectedly, the #4 intake pushrod was bent down near where it goes into the lifter:




Well, that wasn't good.  With the exhaust rocker broken and the intake pushrod bent, it seemed like something could be seriously wrong in cylinder #4.  I got back in Steve's truck and headed back home to pick up a spare pushrod, while thinking about this.  Bent valve?  Broken rod?  It almost seemed like something had to be seriously wrong.

When I got back to the car, the first thing I did was pull the #4 plug.  It looked fine.  Then I spun the motor over while holding my finger over the plug hole, and there was plenty of compression and no leakage back through the intake valve.  Also, the whole valvetrain seemed to be working as it should.  Nothing to do but put it back together and see what happens.  While I was getting the engine put back together, Steve got home from work and mentioned that when he took the broken rocker arm out, it had been sitting vertically in the rocker arm area.  We think now what probably happened was the broken rocker jammed underneath the #4 intake rocker, preventing it from opening, and that caused the pushrod to bend.  In any case, the engine went back together and fired up with no hint of a problem, and I drove home uneventfully. 

I've had to do these kinds of repairs many times over the years, and often in parking lots or on the side of the road.  Drag Week comes to mind.  You guys must have some stories like this; let's hear them!

28
Non-FE Discussion Forum / Support the RPM Act
« on: March 18, 2021, 04:05:38 PM »
Despite my aversion to political issues, this one hits home for any car guy.  Click the link below to generate an email to your congress person about the RPM Act, which allows removal of pollution equipment on race cars.

https://www.sema.org/epa-news


29
Non-FE Discussion Forum / I hate deleting topics...
« on: February 22, 2021, 09:39:18 AM »
And also locking threads, but the political BS is NOT ALLOWED AT ANY TIME on this forum.  I'll start deleting members if I have to...

30
FE Technical Forum / FE Power Cylinder Heads - Results with New Cam
« on: January 31, 2021, 04:57:33 PM »
So after the last round of testing with these heads, we were suspicious that the cam was not really optimized for this engine.  Lykins went so far as to offer to get me a cam at no charge, that he thought would be better suited for the engine.  Not one to look a gift horse in the mouth, I said sure LOL!

Then, after picking out some cam lobes that he thought would work, Brent went to order the cam and found out, to his chagrin and mine, that blanks for FE cams to achieve over 0.800" lift were not available!  Brent called a couple places and so did I, but the only thing that could be done would be to order a custom blank at around $900.  Neither one of us wanted to spend that, so Brent settled on a cam with just under 0.800" lift.  Here are the specs for the original cam that I tested with (the Old Cam), and the New Cam:

Old Cam:  Bullet solid roller, 319/334 Advertised, 285/292@.050", 0.880" gross valve lift on both lobes, 112 LSA, .030" lash on exhaust, .028" lash on intake.  I degreed this cam at 110 ICL.

New Cam:  Comp solid roller, 305/317 Advertised, 276/288@.050", 0.782 gross valve lift on both lobes, 111 LSA, .018" lash on exhaust, .016" lash on intake.  I degreed this cam at 111 ICL.

I sure hope that sometime soon the blanks for more lift on an FE cam become available, but for now all we can do is work with what we've got.  It took me a few days to break free long enough to get the cam installed, but this past Friday I was ready to go.  I had also acquired some new PAC valve springs that were more suited for either of the cams.  Instead of about 1050 pounds over the nose, these were 800 pounds over the nose of the new cam, while still maintaining about 300 pounds on the seat, to get that heavy intake valve closed properly.

Royce and a couple of my friends were here on Friday to help with the testing.  We started off with the existing valve springs still in place.  On startup the first thing we noticed was how much smoother the idle was with the new cam.  Makes sense due to less duration and overlap, but the difference was really noticeable.  After warm-up and lash, we ran the first pull from 3000 to 5000 RPM.  The new cam was so much smaller than the old cam that I wasn't sure what would happen, but as it turned out, the engine did not care about the cam.  Here is chart showing the results from the new cam and the original results from the old cam:




These results were nearly identical, and given the more radical specs of the old cam, at this point I figured that the new cam would make less power up top.  Wrong!  Here is a chart comparing the two cams from 5000 to 7000 RPM:




The new cam actually looks better at the top end than the old cam does.  Go figure...

I'd been anxious to try a valve spring swap on the engine, because those big springs had served their purpose, by proving out the steel rocker arms.  The swap was from PAC 1356 springs to PAC 1224 springs.  I had made a tool to be able to swap the springs with the heads installed, and it took us a couple hours to get that done.  After finishing, we warmed up the engine and ran the first pull from 3000-5000 RPM.  The valvespring swap definitely picked up power, even at the lower engine speeds:




Finally, we worked our way up to the 5000-7000 RPM pull.  Here the difference was even more pronounced:




The torque and HP improvements using the SE heads and the new cam and springs are shown below:

  SE heads, 4V intake, old cam and springs, peaks:  842 HP, 719 lb-ft
  SE heads, 4V intake, new cam and springs, peaks:  849 HP, 724 lb-ft

  SE Heads, 4V intake, old cam and springs, average 3000-5000 RPM:  491.9 HP, 639.6 lb-ft
  SE Heads, 4V intake, new cam and springs, average 3000-5000 RPM:  497.7 HP, 647.2 lb-ft

  SE Heads, 4V intake, old cam and springs, average 5000-7000 RPM:  781.3 HP, 685.8 lb-ft
  SE Heads, 4V intake, new cam and springs, average 5000-7000 RPM:  792.2 HP, 695.6 lb-ft

Peak HP and torque numbers can always be a little misleading, so it's nice to see such a solid improvement in the average numbers as well.


After finishing up with the 4V intake on Friday, Royce and I swapped on the 8V intake.  But after a couple of tests and a jet change, we were down some on power.  Paranoia is always present during a dyno session, so out of an abundance of caution we called it a day.

Yesterday I spent some time going over the engine, checking the valve lash, changing the oil, etc.  Everything looked just fine, and not a trace of an issue when I cut apart the oil filter.  So this morning I reviewed the data that we had collected on the 8V setup  on Friday, and realized that after the jet change our A/F numbers were way lean.  So this afternoon when I ran the engine again I re-jetted to get it right.  Today everything looked good, and we got the same kind of improvements with the cam and spring change as we did with the 4V intake.  Details below:

  SE heads, 8V intake, old cam and springs, peaks:  854 HP, 725 lb-ft
  SE heads, 8V intake, new cam and springs, peaks:  861 HP, 736 lb-ft

  SE Heads, 8V intake, old cam and springs, average 3000-5000 RPM:  474.5 HP, 616.5 lb-ft
  SE Heads, 8V intake, new cam and springs, average 3000-5000 RPM:  486.5 HP, 633.1 lb-ft

  SE Heads, 8V intake, old cam and springs, average 5000-7000 RPM:  786.6 HP, 690.8 lb-ft
  SE Heads, 8V intake, new cam and springs, average 5000-7000 RPM:  795.9 HP, 699.2 lb-ft


It is very interesting to me that the 8V intake is down on power in the 3000-5000 RPM range, compared to the 4V intake.  I assume this is because of the two big Dominator carbs, not really working at the lower engine speeds.  But they definitely take over at the top end.  And 736 lb-ft of torque is 1.44 lb-ft per cubic inch.  That is a really, really good number.

Next on the testing list is testing with the crossram intake manifold, then I'll swap back to the RE heads and repeat everything one more time.  Based on the improvements I've seen with the SE heads, I'll bet the RE heads will peak right around 875 HP.  Not 900, but pretty close, and not bad for heads that have not been ported.

I still have some work to do to to finalize, and potentially improve, the intake manifolds for this package.  But at this point, I have beaten the living SH*T out of the heads, intakes, and rocker arms, and I am quite confident that they will hold up well in a street or race application.  So, I'm pulling the trigger on production as of today.  This week I hope to get current quotes for the castings from the aluminum and steel foundries, plus some of the other vendors I need to get parts from, and then I'll be able to finalize pricing on the package.  If you are on my list for one of the cylinder head packages, I'll be in touch with you in a week or so.  Thanks again to the forum for all the support on this project, I really appreciate it - Jay
                                                                             

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