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Topics - jayb

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196
The Road to Drag Week 2014 / The Road to Drag Week 2014 - August 17
« on: August 18, 2014, 07:37:57 AM »
Just a quick update this week.  Family stuff kept me pretty busy during the week, but on Saturday I got back to assembling the car.  I received my new torque converter from Neal Chance on Friday, and also got some coarse filter screens to put on the dry sump outlets on the oil pan; I had decided that in case of an engine failure I wanted to try to prevent any shrapnel from getting into the dry sump pump.  On Saturday I got the dry sump filter screens installed and the lines modified so everything fit again, and after a certain amount of trouble I got the transmission reinstalled.  Took a lot longer to put it in than it did to take it out, of course... ::)

Sunday I put the front suspension back in the car, which also took quite a bit of time, and then finally mid afternoon I filled the engine with oil, topped off the transmission fluid, and fired the engine.  It ran for 20 minutes with the car still up in the air on the jack stands, and I didn't see one drop of oil or transmission fluid.  What a relief.  I've burned a total of three weeks on this problem; three weeks I didn't really have.  Drag Week starts three weeks from today!

Sunday night I got the wheels back on and put the car down on the scales, after I'd leveled them on the floor, so I could find the CG and get the height set at all four corners.  After I'd made all the adjustments the weight bias was 58/42, much more of a front bias than I'd been hoping for, but it is what it is.  Weight on the rear wheels was pretty close to 50/50 left to right, and the left front wheel was about 120 pounds heavier than the right front wheel.  I think this is about where it should be, given the propensity of a drag car to lift the left front wheel on launch, but I'm not 100% sure about that so I need to do a little research on that this week.

Next I checked the driveshaft angles and found that I had too much up angle on the pinion.  I ran out of time on Sunday to map the four link hole locations, but I'll do that next, get the bars in the holes I want to try to get a neutral launch, and then adjust the bars to bring the pinion angle down somewhat if that is still required.  I think this is going to be Monday night's project.

Last thing I did for the night was put my freshly painted hood in place to get a look at the overall appearance with the hood scoop.  Unfortunately, the throttle linkage that I spent so much time fabricating hits the hood  >:(  I will have to either trim the underside of the hood or revamp the throttle linkage; I haven't decided which yet.

I'm out of time now for testing, so getting to the track on Saturday this week is not optional, it is mandatory.  One way or the other, weather permitting of course, I will run the car next Saturday.  I'll post another update next weekend.

197
The Road to Drag Week 2014 / The Road to Drag Week 2014 - August 10
« on: August 10, 2014, 05:59:47 PM »
This was family vacation week, so there was a limit to how much work I could get done on the car.  After last weekend, though, I didn't much feel like working on it anyway.  Monday morning before we left town I came back out to the shop to check and see if the Loctite sealer had skinned over.  It showed absolutely no sign of drying.  Wondering if it would ever set up, the family and I got in the RV and took off.

All week long I was wondering about the sealer.  We got back home Saturday night around 11:00 PM.  First thing I did was head out to the shop to check the sealer; I really did NOT want to R&R the oil pan again.  Lucky for me, sometime during the week the sealer decided to set up.  Amazing  ::)  Last time I'm using that stuff...

This morning I got out to the shop by 9:00 and got ready to run the engine and check for leaks.  I was still pretty convinced that the leak was coming from somewhere up behind the transmission, but after the last seal and oil pan gasket job I had to check.  After filling the dry sump with oil I ran the test, and sure enough, the oil leak was still there. 

At this point all I could do was pull the transmission, so after the engine cooled down I got to work on that.  It is a tight squeeze up under that car for the Powerglide, and the headers kind of hook around the bellhousing on the bottom, so getting the transmission out is no small job.  I ended up being able to get it out just by removing the right side collector, and jockeying the transmission towards the passenger side as I dropped it.  Took me until 2:00 to get the transmission on the ground, then I used the impact to pull the flywheel bolts and take off the flywheel and the backing plate.  I got up under the car to look with a certain amount of trepidation; I did not want to see everything looking good under there, that was for sure.  Fortunately, the problem was obvious almost immediately:



You will notice that there are two small allen head bolts with washers on them, that function to hold the rear cam plug in place.  Unfortunately, there are supposed to be THREE small allen head bolts with washers, not just two.  One of the allen head bolts was gone.  I reached a small pick up to the hole and poked it through, and sure enough it went right into the crankcase.  Oil splash must have been coming straight out of that hole. 

Now, I'm the one that drilled and tapped those holes for the allen head bolts, because I've had problems in the past on the dyno with aluminum block engines where the cam plug comes out.  So I always use some kind of a retainer mechanism on the cam plug, to keep it in place.  Looks like in this case, though, that little "safety feature" cost me.

Just to double check this, I used the ultraviolet light to try to see some traces of oil in this area.  It had been four hours since the engine had run, but I thought I might still see something with the light.  Boy did I ever:



There was lots of oil coming down across that cam plug, that's for sure.  Next I took out the other two allen head bolts; these are 8-32 bolts, 1/4" long, with fairly large diameter washers to retain the cam plug.  Both of the bolts that were still in there showed evidence of blue Loctite on the threads.  Either I forgot to put the Loctite on the threads of the top bolt, or it just didn't hold for some reason.

Well, at least now I know what the problem was.  But with the trans out of the car there is no way I'll be able to get it back together and to the track next weekend.  One major reason I wanted to make it to the track was to see how the converter behaved, so in lieu of a track day I decided to pull the converter off the transmission in preparation for shipment to the converter place I use.  If you give them engine and vehicle data, they are usually pretty good about getting the converter set up where you want it right out of the box.  I'm going to give them a call tomorrow morning and ask if, with the dyno data I have and the vehicle specs, if the converter I've got will work OK or whether it needs to be modified.  If it needs to be modified I'm going to ship it to them overnight, and hopefully get it back next weekend, so that I can FINALLY get the car all the way together.  All the wiring is done except for some basic cleanup, so once I get the transmission reinstalled and the front suspension back in, I can actually drive the car, which I must say I'm looking forward to.

On another front Steve has been working on the hood scoop, and has the hood pretty much all ready for paint; here's a picture of it sitting on a stand in my paint booth:



Steve plans to get the hood painted sometime this week.  In the meantime, the rest of the car is all apart:



I've got some little things to work on during the week this week, which should finish up the remaining details on the car.  Should be another thrash next weekend, but maybe, maybe, I can get it done.  I'll post another update next Sunday.

198
Non-FE Discussion Forum / US Air Force Museum at Wright Patterson AFB
« on: August 10, 2014, 12:01:56 AM »
Just got back from a family vacation through Wisconsin, Michigan, Ohio, Indiana, and Illinois.  Among other attractions, we spent most of one day at the US Air Force Museum in Dayton.  Always wanted to go there, and finally made it this week.  What an unbelievable collection.  I'll let the pictures do the talking; sorry for some of the poor photo quality, but its pretty dark in some areas, and the place is so big that the flash doesn't light it up:

















































































































If you ever get the chance - go there.  You won't be disappointed.

199
The Road to Drag Week 2014 / The Road to Drag Week 2014 - August 3
« on: August 03, 2014, 09:58:22 PM »
Ever just have one of those weekends where it seemed like everything that could go wrong does?  I'm just coming off one of those  :(   In six months I'll read this post and be able to think objectively about it, but tonight all I can do is think of various four letter words...

On Friday I had planned to be at the track, but after finding the major oil leak in the engine last weekend, and not finding any simple solutions by Monday night, that plan went out the window.  Instead, with my day off Friday I resolved to get the leak fixed.  On Thursday I stopped into my friend BradFORD's shop, and my friend Tom lent me some engine oil dye, and also a UV penlight, to help track down the leak.  Thursday night I got under the car and cleaned everything off with solvent so it was nice and oil free.  I also bent the block plate back towards the flywheel somewhat, so that I had at least a very narrow view of the back of the main cap.  (It dawned on me during this process that the portion of the block plate around the main cap isn't really necessary, and I think that the next time I have the block plate out, I will cut this section away).

I dumped the dye in the dry sump tank, then started the engine and ran it for 30 seconds, then shut it off and crawled back under the car to look for any signs of the leak.  After the fourth 30 second run, I saw a drip running down the back of the main cap.  Looking up into the narrow gap between the block plate and the cap though made it difficult to identify the source of the drip.  I thought it might be coming from the junction of the cap and the block, but it was really tough to tell for sure.  I got back in the car and ran it for another 30 seconds, but when I looked again there was just too much oil down there to identify exactly where it was coming from.  This is a very serious oil leak, with 3-4 drips per second coming out at the back of the engine once it gets going.

After seeing the drip down the back of the main cap I decided that I had no choice but to replace the rear main seal.  Friday morning I got under the car and started disassembling.  With the front suspension on this car, the entire front suspension assembly has to come out to get at the oil pan.  Here's a picture of the front suspension removed, and sitting out in front of the car:



I drained all the oil out of the dry sump and the pan, and saved it because it was new, and I wanted to re-use it because it had the dye in it, and it would be easier to check for leaks with that oil.  After disconnecting the dry sump lines, I pulled all the pan bolts and removed the pan.  After getting it off I took a look at the gaskets and the engine's oil pan rail, and noticed with some surprise that all along the rail there was evidence of sealer and gasket material stuck to the rail, except between the two oil pan bolts that went into the main cap!  There didn't appear to be a good seal to the gasket at that point.  Maybe this was part of the leak issue?

By this time, laying under the dripping engine and the dry sump lines, I was pretty well soaked in oil; this is always a miserable job.  But as long as I was under there I figured I'd finish the job, so I pulled the two #5 main cap bolts and got ready to pull the cap.  On the Shelby block you have to use a slide hammer to get the caps off, but when I tried to fit my slide hammer it hit the floor; it was too long to use in this position.  I had to cobble up a makeshift slide hammer to get the cap off.  After I had the cap off, I grabbed the top half of the seal with a needlenose pliers; it came out easily.

Finally out from under the car, I inspected the cap and seal closely.  It appeared that I had a good seal along the sides and parting surface of the cap, because there was evidence of sealer in these positions.  The main bearing looked fine, and so did the main seal halves.  No real evidence of a problem here.  Hmmmmm...

I let the engine drip dry for a few hours while I did some other work on the car, and then I started the reassembly process.  I made sure to get the pan rail and windage tray nice and clean, free of old sealer, and then spent some time getting dripped on again to get the pan rail cleaned up.  I put the rear main seal in the normal way this time, and clocked the seal in the block just a little to offset the seal gap from the cap gap.  When I installed the cap I put some sealer on the block surface of the cap, as usual.  This time I had decided to try the side seal method that Ross described in another post, so after torquing the cap I installed the side seals with them lubed up with plenty of sealer, and then drove in the nails.  Seemed like it worked just fine.

Finally I got the pan and windage tray installed, using a pair of SCE gaskets that I had ordered this week.  It had occurred to me while cleaning the pan and windage tray that the area on the main cap where there didn't appear to be sealer and gasket residue was exactly the spot on the Fel-pro oil pan gaskets where they fold it in half for packaging.  Maybe that had something to do with the issue, so the SCE gaskets (which don't come folded) should eliminate that possibility.  By around 11:00 PM on Monday I had the oil pan re-installed.  I decided to let the sealer dry overnight, then hook up the pan and fill the engine with oil for the test in the morning.

Saturday morning I was back out to the shop by 9:00, and was ready to test fire the engine by 10:00.  After firing the engine up I watched for a couple of minutes, and no sign of oil.  Great!  The phone rang, and I answered it and talked for a couple of minutes, then cam back to the car and - oh no - another huge puddle of oil in the same spot as before >:( >:( >:(

Well, crap.  Everything had seemed to go together pretty well; why was it raining oil under the car?  I checked again up top, to make sure that there was no oil leaking from the valve covers, heads, or intake manifold, but it was dry up there.  I cleaned off the area under the back of the engine, and went back in with the UV light after running the engine for a minute or so, and this time I didn't see a drip down the cap, but I did see some that appeared to come from the sides of the cap.  But it was difficult to tell for sure; there just isn't much room up there to see what is really going on.

At this point I decided to call a friend of mine who assembles a lot of FEs, and see if he had any suggestions.  His name is Kurt, and after talking this through with him on the phone he volunteered to come over and take a look.  Once he got there I ran the engine again while Kurt watched from under the car, and he agreed that it looked like the rear main and/or the cap to block interface.  So,  we decided to do it all again  ::)

Sparing the gory details of the oil draining and dissasembly, we finally took the rear main cap off again.  I looked closely at the area where the side seals were, and there appeared to be a good track of sealer there, and also at the cap/block junction; disassembling this I would not have expected to see a leak.  Again the main seals looked fine, and this time there was no evidence of sealer missing at the center of the main cap.  It just did not look like there could be a leak here.

Kurt and I took excruciating pains to make sure that the new top seal went in properly, and that the block and cap were perfectly clean and prepped before installation.  This time I did not clock the seal halves like I usually do, but put them in straight because that's the way Kurt likes to do them.  Also we didn't use side seals; we filled the side seal groove in the cap with black Permatex RTV, and then after the cap was installed Kurt pushed into the cavity with a round punch and forced sealer out between the cap and the block, so that we had a bead of sealer coming out the back.  I've done the same thing in the past, using the side seals to force the sealer out.

Kurt left around 6:00, and after a break I came back out to the shop to put the oil pan and windage tray back on (again >:()  After cleaning everything up (again! >:() I decided I would lay a straight edge across the panand make sure the surface was still flat.  Boy, was I surprised what I found.  The back left corner of the pan rail dipped way down, out of line with the rest of the pan rail by a good 1/8"!  How the heck did that happen?  It wasn't that way when I assembled the engine, that's for sure.  I was left with the conclusion that the heat cycles on the dyno had warped the pan, and when I uninstalled it the warp appeared.

Due to the design of the pan it is not possible to hammer this part of the pan rail into shape, so Saturday night I stuck it on one of  my CNC machines, and started re-machining the pan rail.  Turned out I only needed to take about .090" off to get it all squared up.  I got about half way done and the CNC machine quit; it said it had run out of air.  I checked my compressor, and sure enough the circuit had blown and the compressor was off.  I tried to reset the breaker, but it just kept tripping.  So no air compressor, and I couldn't finish the CNC work on the oil pan.

This pretty much just capped off a rotten day.  Earlier in the day UPS had delivered a package to me.  But the package was one I had shipped to a guy in Connecticut with a 351C intake in it.  They delivered it back to me instead!  I called UPS and they basically said OOPS, drop it back off at the UPS store.  Then halfway through the day my daughter had a personal crisis that required a family conference, with lots of wailing and gnashing of teeth.  When the air compressor quit, I'd had it.  I shut off the lights and went to bed.

Sunday morning I was back out to the shop for more punishment ::)  First I flipped on the air compressor breaker, and it fired right up; I think it is getting sensitive to the heat or something, and just needed some time to cool down.  I spent the next hour finishing off the CNC work on the oil pan; while I was doing this I was thinking about the leak, and if this could have been the cause.  When I first saw this issue I thought, aha!  But now I wasn't so sure; the leak had not appeared to be coming from the area where the pan was warped.  Plus, the bolts should have pulled the pan up into position when it was installed; its not totally rigid in that area.  In any case, making the oil pan rail flat couldn't hurt, so after I got done with that I installed the pan.  During this process though I ran out of my favorite sealer, Ford TA-31.  I rummaged around in my sealer box and found an unopened tube of Loctite grey sealer, which I have used successfully in the past, so I finished off with that.  By 11:30 I had the pan installed.  I went back in the house to grab some lunch and let the sealer dry before test firing the engine.

At 1:30 I went back outside.  First I crawled under the car to make sure the sealer had set up, and was surprised to find that it was still not skinned over.  That was odd.  I read the sealer tube, and it said that it should skin in an hour, and be completely cured in  24 hours.  Hmmmm....   I busied myself with some other tasks on the car, and then at 3:30 I crawled back under the car to check the sealer.  Still wet, and not skinned!  I grabbed my heat gun and hit one section of the oil pan where the sealer was pushed out with heat for a couple of minutes.  The stuff was still not skinned, even after that!

Well, I sure wasn't going to try to fire up the engine with the sealer not drying.  I decided to try an experiment.  I dug a bunch of RTV sealer out of my sealer box, including a couple more tubes of the Loctite stuff, and put some beads on a piece of cardboard:



After another hour I checked again.  All three beads from the three different tubes of the Loctite sealer were not skinned, and all four beads from the other four tubes of sealer were nicely skinned over.

So, as I type this, the sealer has still not skinned over, and I haven't yet test fired the engine to see if it still leaks.  I've spent three solid days on this problem, with no resolution yet.  And, frankly, I'm not optimistic about the results of the next test.  In both dis-assembly and re-assembly procedures, I didn't find the smoking gun I was hoping for on the leak.  I'm starting to become pretty convinced that it is coming from the back of the block somewhere, and that next I'm going to have to pull the transmission to look back there.  It could be the cam plug (although I have that held in place with some screws and washers), and it also could be one of the five plugs in the back of the block.  I guess when the sealer finally cures I will find out.  Drag Week starts five weeks from today.  Still waiting to make it to the track...


200
The Road to Drag Week 2014 / The Road to Drag Week 2014 - July 27
« on: July 27, 2014, 11:20:22 PM »
Just a short report this week, plus a video.  I got the rear end gears installed on Wednesday night, and spent Friday night and Saturday until noon getting the throttle linkage worked out.  From there I started working on the wiring, disconnecting all the wiring for the old ems-pro EFI system, and the datalogger electronics that I had added to it, and then working over the wiring for the MS3X that I had put together on the dyno.  Bill Conley was in town over the weekend visiting his wife's family, and he stopped by for a few hours on Saturday night to help out.  Towards the end of the night we had beer and pizza, and Bill snapped this photo of me installing some of the MS3X wiring in the car:



I had no idea that the broad, flat surface of the plenum would be so convenient for holding a couple of beers :D  Anyway, I got most of the way done with the wiring on Saturday night and finished the MS3X wiring up by about noon on Sunday.  After a family commitment I was back out in the shop by 3:00; I still had to install the wiring for the O2 sensor controller and a new relay and wiring for the electric water pump.  Once finished with that I turned on the power, and happily there was no smoke.  After checking out some of the systems everything seemed to be working well except for the Aeromotive fuel pump.  It had flipped on once when I was messing with the wiring, and that was it.  Finally I gave up on that for a while, and finished up under the car, which involved filling the differential with oil, draining the old transmission fluid, installing the pipes and mufflers, and then installing the rear tires in preparation for breaking in the rear end gears.  After that was all done it was around 6:00 PM, and I decided to take the fuel pump and filter arrangement of the dyno and plug it into the car.  Once I did this the fuel system started working fine.  Filled her up with trans fluid and put water in the radiator, and crossed my fingers as I turned the key.  The engine spun over with no trouble, but wouldn't start.  I broke down and hooked the computer up to the EFI system, and realized at once when the display came up that I had not recalibrated the throttle position sensor.  I did that, and tried again, and this time the car fired right up.  Next I wired in the electric fan control, and set up the software to turn the fans on at 180 degrees, and started the engine again.  As it warmed up the idle came up higher and higher, and I still have to address that issue.  The Accufab throttle bodies have the throttle stop screws loctited in place, and there is no additional screw to set the throttle openings, so I had to try to do that with the linkage.  That of course is not the ideal solution, and I'm going to have to work on that in the coming week to find a solution.  But after adjusting the throttle linkage a little more I got the engine to settle into a 1500 RPM idle (?), and warmed it up.  Everything looked fine, so after it cooled a little I took the following video, where I started up the engine again and put the car in first gear to break in the new rear end gears.   The video is not the greatest quality but you will get the idea.  You will also see that there is a lot of cleanup and finish work left to do on the car:

http://youtu.be/DZb7XK9qNMM


After I got done breaking in the rear end gears I felt pretty good about this thing.  Then, I looked under the car, and saw a big puddle of oil with drips coming from the back of the pan  :( :(  I'm a little baffled by this, because the engine wasn't leaking any oil on the dyno, but somehow between the move from the dyno to the car, something has changed.  I started the car up again to try to find the source of the leak but it appears to be dripping all across the back of the oil pan, and the front side of the flywheel is wet with oil.  Its almost like the rear main blew out, and badly at that.  Right up to that point I was confident I was going to make it to the track on Friday this week, but it is leaking so much oil I don't think I dare take it racing.  It looks like I'm going to have to pull the pan.  I will do some more investigation on this tomorrow night and try to figure out where it is leaking; maybe I can patch it externally with some RTV if its not the rear main.  We'll have to wait and see if I can make it to the track or not.  I'll post another update next Sunday...

201
The Road to Drag Week 2014 / The Road to Drag Week 2014 - July 20
« on: July 20, 2014, 06:53:53 PM »
Finally getting closer on this project.  Most of the fabrication work is done, and I'm pretty sure that next weekend I'll be able to fire the engine in the car, and maybe take it around the block a few times.  No way I'm going to be able to hit the track next Saturday, though; right now I'm targeting a test and tune the following weekend.

Last week at this time I was puzzling over my oil filter situation.  The remote filter mount is located up under the left side fender, behind the dry sump tank, and where it ended up being positioned was not ideal; the oil filter wanted to scrape against the fiberglass fender as I installed it, and it was still resting against the fender when it was tightened up.  I was looking for a filter that was smaller in diameter than a standard FE filter to solve this problem (you may have seen my post in the technical section), and after getting some suggestions on this I decided to order one of the FL-400 filters, and also one of the Canton cartridge style filters, to see which one I liked better and would fit the easiest.  The filters arrived on Thursday this week, and I have to confess that I didn't really like either one.  The FL-400 filter was even smaller than I had imagined it would be, and I couldn't see myself running one of those on this engine.  The Canton filter would fit and appeared to be the right size, but when I took it apart I was surprised at how small the filter element was inside.  In addition, the Canton filter didn't have a bypass, a feature which I wasn't real comfortable with.  After mulling this over for a while, I reluctantly concluded that I was going to have to take apart the left front of the car again, and modify the brackets that hold the dry sump tank in order to gain clearance for a standard oil filter.

Also during the week this week I struggled somewhat with the differential.  Last week I brought my pumpkin in to my friend BradFORD for an upgrade to pro gears.  He tried to get it assembled for me on Monday this week, but couldn't get the pinion preload right.  I dropped by his shop on Tuesday, and between the two of us, and a call to Mark Williams, we figured out that the spacer that goes between the pinion gears (where the crush sleeve goes in a standard Ford 9") needed to be machined to fit.  I figured I'd just cut it on my lathe and bring it back the next day, so I took it with me.  Brad had a bunch of shims that he could use to fine tune the width, so he instructed me to cut it .040", which was about .020" more than he thought we needed, and he'd make up the difference in shims.  Tuesday night I got that done (I thought...), and dropped the spacer back off with Brad on Wednesday.  But on Thursday evening I got a call from him, saying that it had not been cut enough, and even with no shims the most pinion preload he could get was 5 inch-pounds.  This turned out to be my fault; I had not measured the spacer before chucking it up on the lathe to cut it, and had relied on the lathe dial indicator to make the cut, since it didn't have to be precise.  But my lathe has a fair amount of backlash, and apparently this screwed up the cut, because when Brad measured the spacer he said I'd only taken off about .013".  I was pretty sure I'd taken off more than that, but Brad measured, and I didn't.  I was already at home when I got the call, so on Friday I had to stop by Brad's shop again and pick up the spacer.  I measured it this time  ::) and got it cut this weekend, so hopefully I'll be able to reassemble the rear end sometime this week.

When Friday night rolled around I got going again on the oiling system.  I pulled the dry sump tank and remote filter mount, and tried to figure out where I could squeeze the tank in closer to the engine compartment, to gain clearance for the oil filter.  This task was complicated by the main forward bar extending from the roll cage and down to the factory frame rail, and a couple other 1" square steel tubing bars that support the front of the left fender and the radiator.  Fortunately, I didn't need a whole lot of clearance.  I ended up removing one 1" square steel tube, modifying the brackets to move them inboard about 1/2", and then remaking the bar that was removed.  This took me Friday night and most of day Saturday by the time I had it finished up, with everything mounted back into position and also the dry sump vent tank mounted.  But now I have sufficient clearance to mount a standard oil filter.  Here's some pictures showing the front left corner of the engine compartment, and also under the left front fender where the oil filter bracket is mounted:





Finally finished with all this fabrication work, I spent the remainder of the evening on Saturday plumbing the car.  I ran all the oil lines, the fuel lines, and the coolant lines from the engine to the remote thermostat housing.  At midnight I finished this up, called it quits and went to bed.

This morning I was looking forward to doing something OTHER than the dry sump system work.  Friday and Saturday nights, while I was working on the dry sump stuff, I also had one of the CNC machines running, cutting out the top for the new upper plenum that I had machined last weekend.  Accufab had come through on the throttle bodies as promised, so those were ready to go.  (I did have to machine the bottom linkage arm off of the Accufab throttle bodies in order to make them fit as low as possible on the plenum top, but this was no big deal.)  Sunday morning I deburred the plenum top and got ready to install the upper plenum and plenum top on the engine.  Here's a couple of pictures of the plenum top:





The second picture is the underside of the plenum top.  I removed the upper plenum that I had fabricated for the dyno work, and got ready to install the new upper plenum.  Here's a picture of the engine ready for the upper plenum installation:



Naturally, when I went to install the upper plenum, it didn't fit LOL!  It turned out that the fuel line fittings were too close to the outer walls of the upper plenum.  Glad I had already installed those; otherwise I might have had to take everything back apart again when installing the lines.  Back to the CNC machine with the upper plenum; I relieved the outside wall in four places by about .050", to clear the fuel line fittings.  Back to the car, and this time the upper plenum slide right into place.  After bolting it down and using plenty of Loctite on the screws holding it in position, I cut an O-ring to fit around the top.  Here's a picture of the upper plenum installed:



Next I bolted on the plenum top:



Finally I put some carb studs in the plenum top and installed the Accufab throttle bodies.  Unfortunately, when I tried to open the throttles the linkage interfered with the plenum top.  I had known about this and countersunk a couple of holes into the plenum top for clearance, but I was just off a little bit on the hole locations, and the linkage hit when the throttles were open about 25%.  Back off came the plenum top, and back over to the CNC machine to enlarge the holes.  I checked the throttle linkage clearance while the plenum top was still fixed in the CNC machine vise (something I should have done the first time around), and now I had plenty of clearance.  So, back on went the plenum top, and finally the Accufab throttle bodies were installed:



By this time it was early afternoon, but now I was ready to install the hood and see what the clearance situation was like.  With the previously fabricated plenum and the Wilson throttle bodies, the hood would not fit down all the way onto the car.  My new plenum and Accufab throttle bodies reduced the overall engine height by 2", but when I installed the  hood it still wouldn't fit into place.  Turned out that the extra width of the new plenum was hitting some of the original fiberglass in the hood, and fortunately it was underneath the hood scoop, so I just removed the scoop (which is a currently bolted on), and trimmed away the offending section of the hood.  After reinstallation the hood fit fine; here's a picture of the throttle bodies peeking through with the scoop removed:



After re-installing the hood scoop I measured the clearance between the underside of the scoop and the top of the throttle bodies; it was 1 3/4".  I wanted at least 3" of clearance, so I made up some 1 1/4" spacers and bolted the hood scoop back in place, with it spaced up, to check everything.  This looks like enough room over the throttle bodies to me; what do you guys think?



Finally today I installed the radiator, hooked up the electric fans and the trans cooler, and fabricated a lower radiator hose to fit around the dry sump pump and hook up to the CVR water pump.  Then just for grins I temporarily installed the grille.  This thing is finally starting to look like a car:



I still have some fabrication work to do, including making up the throttle linkage and making a plate to seal the scoop to the plenum top.  My pal Steve, who is going with me again this year to Drag Week, is a bodyman extraordinaire; he is taking the hood and the scoop, and will be fiberglassing it together in the raised up position, then getting the bodywork and paint done over the next few weeks.  He has promised me that the bodywork will be finished and the hood in primer in time for me to make it to the track in a couple of weeks.  Other than these items, the time consuming fabrication work on the car is pretty much done.  I did not get to the electrical stuff this weekend, but I'm thinking I can knock that out this week and next Saturday, so Sunday I should be able to start the car, break in the new rear end gears, and maybe go for a hoodless test drive.  I'm looking forward to that!  I'll post another update next weekend.






202
FE Technical Forum / FE Oil Filter with Reduced Outside Diameter?
« on: July 16, 2014, 02:40:30 PM »
I'm pretty sure that I've seen an oil filter that will fit an FE, but has a smaller outside diameter; anybody know who makes such a thing, or have a part number?  Where the oil filter adapter is on my race car there is limited room, and having a filter that is smaller in diameter by 1/2" or so would make it much easier to service.  Thanks in advance for any help on this - Jay

203
The Road to Drag Week 2014 / The Road to Drag Week 2014 - July 13
« on: July 13, 2014, 08:16:21 PM »
Last Sunday night I had set a schedule for getting to the track in three weeks, and that schedule called for me to be pretty much done with the mechanical work on the car this weekend.  I was going to get the electrical work done by next weekend, and have the car running and driving, so that by the following weekend I could go to the track.  Unfortunately that schedule went out the window almost immediately this week, for a variety of reasons, including lack of availability on the Accufab throttle bodies, and the need for some rear end components to match up with the pro gears I'm installing in the car.  Also, the garden variety stuff I needed to get done to get the car assembled took a lot longer than I expected, so I'm still pretty far from having it put together.  Nevertheless I did get a lot accomplished; just not enough.  I would say at this point that making it to the track on July 26 is questionable, but I will keep plugging away and see what happens.

After doing an inventory of the parts I needed on Sunday night, I made the calls at lunch on Monday to get the rear end components I needed, and the Accufab throttle bodies.  I called Accufab first, and found out that they were out of stock.  After calling a bunch of their distributors I found that none of them had the throttle bodies in stock, so I called Accufab back and placed the order.  They say they will be shipping tomorrow (Monday), but we will see.  Since I wasn't going to have the parts to get the car mechanically completed, I elected not to pay for next day air for the rear end parts that I needed from Mark Williams; those shipped on Monday but did not arrive until Thursday.  Friday at lunch I took all the rear end components over to my pal BradFORD, and he should have the pumpkin ready to go with the pro gears by the middle of this week. 

I also planned to revamp the plenum of my intake to make it lower, but maintain about the same volume by making it wider.  After figuring out exactly what I was going to do on Monday night, Tuesday I ordered a couple of hunks of aluminum plate, one 12" X 22" X 1/2" piece for a new top plate, and one 12" X 22" X 2" piece for the new plenum spacer.  Most of this material is going to be machined away, of course, but I decided to machine it from a solid piece rather than weld some smaller pieces together, because I suck at welding aluminum, and I'm pretty good with the CNC  ;D  The aluminum dealer told me I could pick up the material on Friday.

As usual time was short to work on this project during the week, and Friday night the wife had plans for me, but Saturday morning I got going early.  Last weekend we had just dropped the engine and transmission into place, so the first thing I did was crawl under the car to put the motor mount bolts in.  You'd think this would be relatively painless, but of course it wasn't.  I had purchased new motor mounts for the engine, and apparently the distance between the flanges on the mounts, where they fit over the frame mounts, were significantly smaller than the frame mounts themselves.  The engine was probably up 1/2" over where it needed to be, and the weight of the engine wasn't enough to put the mounts down into position.  I struggled with this for quite a while, and finally ended up using a big C-clamp to pull the mount down into position over the frame mounts.  I had to point the ends of the motor mount bolts and pound them through to get them into place, but finally after about two hours I had the engine bolted down.  Sheesh, what a battle; the only positive thing on this was that the engine was actually sitting a little lower now.

Next I took a little break, and programmed one of the CNC machines to start cutting out my plenum spacer.  Here's a picture of the top side being cut:



That picture was taken after the center was cut out of the 2" thick plate, and the angled sides of the plenum spacer are being machined.  Sure were a lot of chips from that little project LOL!

After getting the CNC machine running I got back to the car, and the next project, which was to put the steering rack and lower control arm mount up into position.  This one is always a pain on this car, and let me warn anybody who is thinking about a Fat Man Fabrication strut conversion setup for an early Mustang that it is not a good kit, doesn't fit well, moves the wheels inboard 2" without telling you, etc. etc.  There are two big 1/2" through bolts that go through the rack and lower control arm mount, and also go through the original Ford lower control arm mounts on the car.  As you install the bolts you need to put three spacers on each side in place, and there's not a lot of room to work, so you end up doing this kind of blind.  And of course you have to assemble the steering linkage while you are doing this.  Another three hours of horsing around and I finally got this stuff all finished up.  Next up were the headers, which are also a very difficult installation on this car.  The biggest issue is getting the headers themselves to line up with each other and hook together.  There are twelve separate pipe sections on these headers, with tabs holding them together, and as you install them in the car, for some reason they don't like to line up with each other.  They were easy on the dyno, but the car presents a whole new set of problems.  I got the left side done, and a start on the right side, before midnight rolled around and I decided to call it a night.

Sunday the first thing I did was flip the plenum spacer over in the CNC machine so I could machine the bottom side.  This took a while, but finally around 6:00 PM it finished up.  Here's a picture of the completed spacer:



When I get the Accufab throttle bodies, hopefully this week, I can do a drawing and machine the top plate, and then the induction system will be ready to go.

Next I got going on the right side headers, and by noon I had that side finished.  I spent the rest of the day today modifying the front left corner of the car, fabricating a mount to fit the dry sump tank, remote oil filter, and breather can.  This also took a lot longer than I thought (imagine that), but by the end of the day today I had that pretty much under control.  The following picture shows the dry sump tank; behind it out of sight and up under the fender is the remote oil filter adapter.  I still haven't done the mount for the oil catch can, but I know where its going to go and it shouldn't be too tough to get that mount finished up.



Finally here's a picture of the engine in the car, as it sits right now:



Next week if all the parts come on schedule I should finally have the mechanical work done on the car by Saturday.  This leaves me Sunday to do the wiring, get the car running, etc. etc.  Don't know if I'll make that or not, but I will do my best.  I'll post another update next weekend.

204
The Road to Drag Week 2014 / The Road to Drag Week 2014 - July 6
« on: July 06, 2014, 10:04:46 PM »
The three day holiday weekend really afforded me a great opportunity to make some headway on this project, and I was fortunate enough to take advantage of it, without a lot of family commitments this weekend.  Right now I've caught up some on my original schedule, and it looks like I'm only about three weeks behind.  My original plan was to have the car running and driving this weekend, but now I'm thinking that I'll make my first trip to the track on July 26.  There are another 2 or 3 track days that I can squeeze in before Drag Week after that point, so hopefully this will give me the opportunity to get the car really well sorted.

Once again I was tied up during the week this week, but on Friday morning I got going right away on the engine.  I still had several things I wanted to try on the dyno, primary among them getting the crankcase sealed, and retesting without the 1/2" plenum spacer I had installed last weekend.  The plenum spacer was kind of a head scratcher for me.  Before installation of the plenum spacer, the dyno data had been showing a vacuum in the plenum of up to 0.6 inches.  When I installed the plenum spacer the vacuum during the pull went to zero, but the engine picked up kind of a funny pulsing noise partway through the pull.  It also picked up power.  I was pretty sure that the pulsing noise was induction noise, but I hadn't heard anything quite like it before, so I wanted to run another test, to remove the plenum spacer and see if the noise went away again.  Also this week my new O-rings arrived, which were larger in cross section than the original O-rings; I hoped that they would provide a better vacuum seal around the spark plug tubes for the dry sump system.

Also, over the course of the week I had carefully reviewed all the datalogs from the cam sensors, and had concluded that in all cases, regardless of the sensor and target combination, the right cam was retarding about 3 degrees more than the left cam.  Whether I believed the absolute numbers or not, this phase shift between the two cams seemed pretty consistent, and also dovetailed with my original test data from 2006.  So, after thinking it over I elected to advance the right cam 3 degrees with respect to the left cam.  This put the cams at 105 and 108 for ICL, which was exactly where I had set them when I set the cam timing on the engine stand, before the engine went on the dyno.  It kind of felt like all the cam timing changes I had done were a wasted effort after this, but at least the way I've been setting up the cams on these engines over the last 7 or 8 years has probably been correct.

So on Friday I tore the top end of the engine apart, to advance the right cam 3 degrees, check the timing chain tension, give the valvetrain a very close inspection and reset the lash, etc.  I also removed the Honeywell sensors from the valve covers and replaced them with Cherry sensors, which were the ones I planned to run in the car.  I made sure to seal them with some RTV from the inside, because the Honewell sensors had shown leaks around this area.  Thinking about the crankcase sealing issue I decided to take a new set of cork valve cover gaskets and glue them to the valve covers, to help hold the gasket in place when vacuum was being developed in the crankcase.  I decided to let the sealer dry overnight so that on Saturday morning I could pressurize the crankcase again and check for more leaks.

I had still also wanted to run a pair of Dominator throttle bodies on my sheet metal intake, so I spent the rest of the Fourth of July holiday (until the fireworks started at 9:30) working on a new top for the intake.  First I drew up the design for the top in my CAD software, and then wrote the program to machine a piece of 1/2" aluminum plate to the drawing.  While the CNC machine was running I robbed the two Dominator throttle bodies off the high riser in my Mach 1.  Around dinnertime I had the plate finished up; here's a couple of photos, one from underneath (the inside of the plenum), and one from on top showing the throttle bodies bolted in place:





To be honest I didn't really think the Dominator throttle bodies were going to help much, because the 90mm throttle bodies flowed 1100 cfm each, but it was worth a try, especially since I didn't have to buy any parts to try it.  After I got the top done I took some spare 1" X 3" aluminum angle and welded it together into a box that would fit on top of the intake, then welded the top plate in place.  At the end of the day on Friday I was pretty much ready to go with the Dominator parts.

Saturday morning I finished re-assembling the engine on the dyno, without the 1/2" plenum spacer.  Then I ran the pressure check again, putting 5 psi into the crankcase.  I was pleased to see that the leaks around the spark plug tubes were gone, and also that there were no leaks around the cam sensors.  I began checking the rest of the engine over, and then discovered a leak that I hadn't seen last weekend.  This one was between the intake manifold and the head.  Now, on a regular FE I would never have had to worry about this because this junction is covered by the valve cover, but on the cammer of course this is not the case.  I had run a ring of RTV around the ports on either side of the intake gaskets, but as I sprayed a soapy water solution onto the junction between the intake and the heads, I could see that pressurized air was escaping past the gasket and between the ports.  And some of these leaks looked pretty substantial.

I dug out the Ford TA-31 and ran a bead of it along the top of the intake manifold rail and down the sides a little ways to try to get this area sealed up.  I decided I wanted to let this cure for a couple hours before running the engine, so I took care of a few other things in the shop while I waited.  About noon Marc Hunter from the forum came by; he was in Iowa visiting his brother, and had previously arranged to stop up to my place and pick up his FE intake adapter.  He brought his brother Ryan with him, and his dog, named Cammer.  Best name ever for a dog if you ask me LOL!  Ryan owns SCE gaskets and is working on some new FE gaskets, and wanted to show me some of the stuff he was doing and ask a couple of questions.  I told him about some SOHC gasket requirements that I would like to see, including a valve cover gasket that isn't cork, and also gave him one of the old Victor Reinz FE intake gaskets, which were far and away my favorite FE intake gasket until they quit manufacturing them.  Maybe SCE will start making them now.

After a quick tour of the shop and some more technical discussions I got back to working on the engine, while Marc and Ryan hung around waiting for me to be finished so they could see the engine run on the dyno.  I still had to wire up the new Cherry sensors I'd installed in the valve covers, and this took about an hour to finish up.  Finally around 2:00 or so the engine was ready to go.  It fired right up as usual, meaning that I hadn't screwed anything up with the cam sensors (which is always a possibility LOL!).  A couple of minutes into the warm up it dawned on me to look at the crankcase vacuum, and lo and behold, I had close to 10 inches of vacuum running at only about 1500 RPM!  Boy I felt good about that; all the chasing around of the vacuum leaks had paid off.  I was pretty sure that significant crankcase vacuum would improve the power output of the engine, so after the warm-up was complete, I made another 5500-7500 RPM pull.  The first thing I noticed during the pull was that the noise from the previous few pulls was gone; removal of the plenum spacer seemed to have eliminated that sound.  After the pull was over and we looked at the data, sure enough the 0.5 inches of manifold vacuum was back.  So the plenum spacer definitely helped the power output, and caused the new noise.  But on this pull, I was a little disappointed by the power numbers.  It seemed that the crankcase vacuum had not improved power at all!  This was a surprise, given the size of this engine and the low tension rings I'm using.  A review of the data showed that 10 inches of vacuum was all I was getting.  I figured that I could use up to 20" or more, so after talking it over with Marc and Ryan I decided to adjust the vacuum relief valve on the engine to stay shut until a higher vacuum level was reached.   I started the engine to run another pull, but now the crankcase vacuum was reading much lower, maybe only 1-2 inches.  I was confused by all this, but I ran the pull anyway.  Towards the end of the pull some smoke starting coming from the right side of the engine, indicating a valve cover leak.  The engine didn't seem to care, though, and made the same power as the pull before.  After looking at the data we went back out into the dyno room and I checked the valve cover bolts.  Sure enough, some of them were really, really loose.  This is one reason why I would like to see a rubber or composite valve cover gaskets for the SOHC; the cork gaskets get hot, shrink, and then start leaking.  Then, as you tighten down, the same thing happens a few more times.  Finally after you've tightened them a few times the cork splits and you have to ditch the gaskets and start with a new pair.  A better gasket for the valve covers would be a real help for these engines.

After tightening the valve cover bolts the crankcase vacuum came back.  Marc and Ryan had to make the return trip to Iowa; two really nice guys, and it was my pleasure to have them visit.  After they left I took a short break and then went to the next test, which was to install a 1" plenum spacer on the intake.  I figured if a 1/2" spacer was good, maybe a 1" spacer would be better.  I was curious what the engine would sound like with a 1" spacer, but when I ran the test it sounded the same as with no spacer at all, and the power was back down a little, plus the 0.5 inches of vacuum was back in the plenum.  So it seemed like the 1/2" plenum spacer was optimal for this engine. 

At this point, I decided to install the new plenum top with the Dominator throttle bodies.  Here's a picture of the engine with these installed:



As mentioned previously I didn't hold a whole lot of hope out for this combination, but I thought I would give it a try.  Boy, was I mistaken!  The Dominator throttle bodies picked up a solid 20 horsepower over the entire RPM band, 5500-7500!  A huge, huge power improvement.  Boy, was I happy to see that!

It was getting towards the end of the day Saturday, and I had wanted to run some more experiments with the Dominator throttle bodies by adding some plenum spacers, but I was running out of time to do that.  I decided to jump to my last test.  During all the testing with this engine I was seeing about 0.85 psi in the dyno's exhaust system.  Usually there is power available when there is pressure in the exhaust system; in fact, I documented some of this in the miscellaneous testing section of my book.  So, for the last test I disconnected the exhaust system and ran the headers open in the dyno room.  When I started the engine, I immediately had to put ear protection on; that thing was LOUD.  I ran the pull, and anxiously downloaded the data and...  no improvement.  Nearly identical numbers to the previous pull with the exhaust system connected.

So the dyno results this weekend were all rather surprising to me.  First, no power improvement with vacuum in the crankcase.  Second, a big power improvement with the Dominator throttle bodies.  And finally, no power improvement with open headers over the dyno exhaust system.  I would not have guessed any of these outcomes.  I guess all this shows is that you have to test this stuff to really find out the truth.

Sunday morning I spent working on the car.  It felt pretty good to get my hands back on it; it has been two years since I've really done anything with it.  I got it positioned in the middle of the shop and spent some time pulling the pumpkin, because the car currently has street gears in it and I need to put in a set of pro gears.  Shortly after noon my friend Kevin R came by to give me a hand pulling the engine off the dyno, and putting it in the car.  We attached the engine and transmission together, along with the Gear Vendors overdrive, and had it muscled into place by 4:00.  Here's a photo of the engine in position:



Right away I could see that my hood scoop is too low, but I have some plans to address that, including getting a pair of Accufab Dominator throttle bodies, and reshaping the plenum box to make it wider and shorter, so it has the same volume but a lower profile.  I have a lot of work in front of me on the left front corner of the engine compartment, to fit the dry sump tank and accessories, but I think I can get all this done in the next couple of weeks.  I'm shooting for a test and tune at a local track on July 26; we will see what happens.

205
The Road to Drag Week 2014 / The Road to Drag Week 2014 - June 29
« on: June 29, 2014, 09:40:11 PM »
Another good week on the project, and a good weekend on the dyno this weekend.  After last weekend I was intent on trying to figure out the cam advance/retard situation with the cam sensors, so last Monday I ordered some more of the Honeywell cam sensors that I had used for this purpose back in 2006, along with some of the required triggering magnets.  These sensors pick up the presence of the magnet as it spins by the sensor, and provide a high speed digital output.  The magnets come in a little aluminum carrier with an 8-32 stud on the back, so all I had to do to mount them was to center drill and tap one of the bolts on each cam that holds the cam sprocket on.  Then the magnet carrier and magnet screw right into place.  Here's a picture of one of the magnets mounted on the cam sprocket:



After that I mounted the new sensors in the valve covers and set the airgap at about .060".  I had also wanted to make sure that I ran the two sensors off the same set of electronics, in case different voltage supplies or noise was causing one to be thrown off compared to the other.  So along with the magnets and sensors I picked up some other assorted electronics and made up this little circuit as shown below:



The device with the three legs is a common voltage regulator, with input voltage up to 30V and a 5V output.  The two yellow things are capacitors that are required when using the voltage regulator.  Then there are two resistors, and two LEDs, one set for each of the sensors.  I fit these together into a little plastic box:



With this arrangement I wired both sensors to the same 5V power supply and ground, and wired each sensor output into the resistors and LEDs, and then also fed each output into the MS3X control unit.

By Friday night I was all finished up with the electronics stuff, and decided to try another cam timing change.  My last change had been to advance the right cam from 105 to 102, and the left cam from 108 to 102.  This had resulted in a loss of about 20 HP, so I elected to go back a little, but keep the cams equally phased.  Working VERY carefully on Friday night, I got both cams backed up to 105.  On Saturday morning I fired the engine and ran the first test.  Thankfully power picked back up to the original level, or very close to it, but again the cam datalogs were confusing.  For the left cam, I was observing about the same thing that we observed last week, but the right cam looked much. much better.  It actually looked way TOO good, and was hardly moving at all during the warm up or the pulls.

For the cam sensor I am using two inputs to the MS3X.  The first input is dedicated to a cam sensor, and the second is an auxiliary input.  The left cam was on the cam sensor input, and it looked pretty much the same as last week, but the right cam did not.  After a little reflection this was even more puzzling, because last week, with different sensors, I was getting results on both inputs.  Really scratching my head on this one.  After a few more pulls and basically repetitive results, I called Scott Clark to ask him about this.  Scott suggested that I swap inputs to the MS3X and run another test.  I did this, and sure enough, now the right cam sensor looked like it had a believable signal, but the left cam sensor didn't.  This basically proved that the MS3X auxiliary input was smoothing or modifying the signal, rendering it useless.

At this point I made another change to the cam timing, moving both cams to an intake centerline of 108.  The LSA of these cams is 114, so now both cams were degreed 6 degrees advanced.  On the next pull I picked up a little more power, but not much, around 1.5 HP average across the 5500-7200 RPM range.  According to the cam sensor datalog, the left cam was retarding 9 degrees as I went into the dyno pull, and then retarded a further 5 degrees during the pull from 5000-7200 RPM.  That would mean that the effective intake centerline angle of the left cam was 8 degrees retarded, or 122 degrees, to make peak power on this engine. 

I just didn't believe this; that is so far out of whack with what I know about engines that it just doesn't pass the smell test.  After reviewing the data from both cams (including from the right cam when it was being logged by the cam sensor channel), I think one thing that I do believe is that during the pull, both cams are retarding about the same amount, 5 degrees or so.  It the data prior to the pulls is disregarded, that would put the existing timing of the cams as about straight up, which makes more sense from a power perspective.  I decided at this point to just abandon the cam logging experiment; I was chasing horsepower anyway, not cam angles.  I'm going to do some more experimenting with the cam timing next weekend, but I'm pretty close to dialed in at this point.

Now, with both cams at about 108, I decided to try another test.  I pulled the throttle bodies off the front of the intake and put them on top.  Here's a picture of this arrangement:



The motor definitely liked this change, picking up 10-15 horsepower across the top end power band, and not losing anywhere.  I kinda figured it would like that.  This also had an unexpected effect; prior to this pull, all the previous pulls had shown zero vacuum in the plenum.  But with the throttle bodies moved up top, suddenly I had 0.5 inches of vacuum in the plenum above 6500 RPM.  Apparently the engine was drawing the air more efficiently now and the throttle bodies were a restriction.  However, sometimes plenum volume plays into this kind of thing, and I had my second 1/2" plenum spacer ready to install.  Current plenum volume is 580 cubic inches with the first spacer, and the second spacer would increase that by 60 cubic inches.  So, I took some time and got the second spacer installed.  Here's a photo of the manifold with the top removed and the first spacer visible.  I machined these out of black Delrin, and cut them for an O-ring to make sealing them up easy:



After the installation the next pull got me another 7 average horsepower across the speed range, and back to zero vacuum in the plenum for the whole pull.  Along with that the engine seemed to be running a little leaner, so over the next few pulls I richened the top end up about 4%, and picked up a few more horsepower.

Throughout this whole process I still was not seeing any significant amount of crankcase vacuum.  I decided I needed to track that down at this point.  I have an electric vacuum pump that I use for vacuum forming, and I attached that to the crankcase to try to pull a vacuum on it, and then hold a lit cigarette near any potential leak spots to see where the smoke gets sucked in (cigarettes courtesy of my pal Steve P, since I don't smoke).  This just didn't seem to work too well; I think that the vacuum pump doesn't pull enough volume to make it all the way around the engine, so the smoke from the cigarette didn't react to any leaks.  Also, I felt a little nervous holding a lit cigarette a few feet from the dyno's fuel tank LOL!  Anyway, my Y-block pal JC was over this afternoon, and he suggested the opposite approach, pressurizing the crankcase to 5 psi or so to see if we could check for leaks with a soapy water solution.  This approach gave instant results, and I found some fairly major leaks around the spark plug tubes.  I was using 2 O-rings to seal each tube, but either that wasn't enough or the O-rings were old or something, because air was going by all eight of those things in a big way.  I also found leaks around the cam sensors that were screwed into the valve covers, and around the valve cover rails themselves.  So, this week I'm going to work on getting those leaks sealed up and see if I can develop some more crankcase vacuum.  There is certainly some power to be had there, because this engine is large and has low tension rings.

At the end of the day today I ran one last pull for the camera.  At the end of  the pull a drop of oil drips on the right side headers and generates some smoke, but otherwise the pull looks pretty good.  This is the engine running from 5500 to 7500 RPM:

http://youtu.be/1BxFC2B7ZSk

I'm going to give myself on more weekend on the dyno with this engine to try to tweak it just a little more, then its going in the car.  In fact, with the 3 day weekend coming up, I might just take it off the dyno and try to get it in the car on Sunday.  I'll post another update next week - Jay

206
The Road to Drag Week 2014 / The Road to Drag Week 2014 - June 22
« on: June 23, 2014, 12:37:55 AM »
Dyno weekends tend to be exhilarating and frustrating all at the same time, and this one was surely that!  When I wrote my last update I figured I'd be spending all weekend wiring the EFI system onto this engine, and would be lucky to get it running.  That all went out the window on Monday when I emailed Scott Clark and told him that I probably wouldn't be ready to run this weekend, because I didn't have the engine wired and I wanted to have it up and running before he drove up with his double throwdown, triple whammy 8 oxygen sensor tuning setup.  But in his return email Scott pointed out that he was not tied up on Friday, and if I could take Friday off he would come up and help me wire the engine, and we could get it running and tuned over the weekend.

Well, I had another errand that I had to run on Friday morning anyway, so I had already taken the day off.  Scott had to drive up from Omaha to my place, and I figured with both of us working on the wiring we might be able to knock it out by the end of the night on Friday.  So we made the arrangements, and I spent some time during the week getting all the mechanical stuff done for getting the engine running on the dyno.  On Thursday night I was clipping part of the wiring harness out of my Shelby clone and putting it in place on the engine, and at the end of the night on Thursday, for once it appeared that I had overestimated the time it was going to take to get the project done; it seemed like between the two of us Scott and I could indeed get the wiring done on Friday.

Friday I got back from my morning errand by 11:00 or so and started working on the wiring shortly thereafter.  Scott showed up around 2:00 and between the two of us we had it finished up and were ready to start the engine by 6:00 PM.  About that time another guy that Scott knows, Mark Dahlquist, also showed up.  He drove down from Fargo ND to meet up with Scott and drop something off with him, and he hung around to help out with the engine.  I was really lucky to have both of those guys here to help out.  Some of you may know that Scott is kind of the EFI tuning guru for a lot of motorsport teams; he tunes for Bischoff and Ray Barton at Engine Masters, and of course those teams always do well.  He also tunes for some of the Bonneville teams, and he is actually making his living at this point tuning engines.  I hadn't met Mark before this weekend, but he is also an Engine Masters competitor; his first year was last year, and he finished 9th (I think) with a Pontiac engine, with Scott tuning the engine for him.  The most recent issue of Popular Hot Rodding has a writeup on Mark's EM engine.  Talk about qualified assistance!  I'm practically a newb compared to these guys.

Anyway, after Mark showed up Scott spent some time setting up the Megasquirt MS3X EFI system, and then we tried to start the engine.  First time out on this stuff you are always concerned about getting a good signal from the crank sensor.  I was using a Ford VR sensor on the crank target wheel, and a Cherry digital sensor for the cam position sensor.  After several tries we got the engine started, but I shut it off right away because we hadn't put coolant in the engine yet.  When assembling this engine I had been concerned about internal water leaks, so I had decided that the first thing I was going to do was to run the engine on the dyno with a radiator, so that after the water temp came up I could dump in some Moroso ceramic sealer and circulate that through the engine for a while to seal up any seepage that might be present.  After we knew the engine would start, I got to work setting up the radiator and the cooling hoses.  Mark had the idea to put some hooks in the ceiling and hang the radiator from a couple of tie down straps; that worked out very well, and shortly thereafter I had the cooling hoses attached to the water pump and the thermostat housing, and the electric fans wired up.  I filled the engine with distilled water at that point, checking carefully for any leaks, but there weren't any, so that was a good sign.

Next we fired up the engine, but Scott was concerned about the crank signal because the engine wasn't running that well.  The MS3X system has a diagnostic mode where you can watch the signal from the crank sensor, after conversion to a digital signal (the Ford VR sensor puts out an analog or sine wave signal).  This is just like having an oscilloscope screen on your computer so you can watch the crank and cam signals.  This diagnostic mode was showing errors with some of the teeth on the target wheel; the sensor was losing teeth, and so the missing tooth on the wheel was not being detected properly.  We messed around with the sensor airgap to try to resolve this problem, and it seemed like it mostly went away, but still would give us some intermittent errors when the engine was running.  In any case though, we could get the engine started, and it sounded pretty good.  Finally around 10:00 PM we just decided it was getting too late and that we needed to run the engine to get the sealer circulating; I didn't want to leave it overnight with water in it and no sealer, and also I wanted to circulate the sealer and then later drain the coolant out of the engine, per the sealer's instructions.  So, we fired it up with a less than ideal crank sensor signal and started warming up the engine.  It wouldn't idle much below 1500 RPM at this point, but that was OK for Friday night's purposes.  After the engine was warmed I dumped in the bottle of sealer, put the cap on the radiator, turned on the electric fans, and let the engine run.  The CVR water pump seemed to keep right up with the cooling system; it did gradually warm over 30 minutes from 180 degrees to 210 degrees, but by that time the sealer was well circulated and we had run the engine twice as long as was recommended by the sealer instructions, so we shut it down and called it a night.  Scott and Mark took off, and around midnight I came back out to the shop, drained the water out of the engine, and then went to bed.

Saturday morning I was up early, taking the radiator off the engine and hooking up the dyno's cooling system.  After Scott and Mark arrived back we got to work on the startup procedure for the engine again.  We continued to have trouble though with the crank signal.  For a while it would work just fine, with no errors, then suddenly we would get bunches of errors all at once, and the engine would sound like crap.  One thing we tried was changing the lead on missing tooth of the crankshaft target.  My target wheel, like the Ford ones, has a tooth every 10 degrees around the wheel, with one tooth missing to allow the EFI unit to sync up to the wheel, and know where top dead center is.  I had the tooth #1, which is the first tooth after the missing tooth, set for around 65 degrees BTDC.  My target wheel is drilled for multiple mounting positions, in 20 degree increments, so we tried advancing the target wheel so that tooth 1 was at 45 degrees, and retarding it so that tooth 1 was at 85 degrees, but still couldn't get a good consistent crank signal.  This was the same issue that was dogging me at Drag Week in 2011, so we really needed to get this problem solved.  Scott began promoting use of another Cherry digital sensor, like the one we were using for the cam sensor, on the crank; he had recently had good luck with those.  I did have one spare Cherry sensor, so finally I installed one in place of the Ford VR sensor.  There was an immediate improvement in the cranking signal from the sensor, and the engine began starting much more easily.  We had it up and running for several minutes at a time while Scott tuned the A/F ratio and logged the sensor diagnostic data.  We were still seeing some drop out of the crank signal, though, so Scott thought we should try moving the target wheel again.  After I did that, suddenly we had nothing for signal, and the engine wouldn't start.  Mark went into the dyno room and wiggled the sensor, and found that it was loose!  This was my fault; I had only put the nuts that held the sensor in place finger tight, and they had come loose and the sensor had started to wobble around.  I tried to put the sensor back in its original position, but it looked like the sensor body had been dinged by the target wheel, and it just wouldn't work anymore.  So, our crank sensor was no longer working. 

We thought about going back to the Ford VR sensor, but I did have a couple of other digital output sensors made by Hamlin that would also work.  Unfortunately the Hamlin sensors wouldn't physically fit in the crank sensor mounting bracket that I had machined for this engine.  So, in the end what we decided to do was take the Cherry sensor out of the left valve cover, use that one as the crank sensor, and put one of the Hamlin sensors into the valve cover to act as the cam sensor. 

All this screwing around with the sensor took the whole morning and most of the afternoon, but when we got the new sensor configuration set up it seemed to work really well.  Finally we were ready to make some dyno pulls.  We started with pulls from 3000-5000 RPM, and gradually worked our way up to 5000-7200.  The engine sounded really good, but was down just a little bit on power compared to what I was expecting.  (By the way, this will be disappointing for some of you guys but I won't be sharing any of the dyno results from this engine just yet.  There are Drag Week competitors watching this web site, and I don't want to tip my hand before the event.  I will post the dyno results on this blog in September, after Drag Week has started.)  While we were doing these pulls Scott was messing around with a software feature in the MS3X called VVT.  VVT stands for variable valve timing, and it allows the MS3X to control the variable valve timing actuators found on some modern engines.  What he was discovering, though, was that despite the fact that this engine doesn't have VVT actuators, the MS3X can log the position of the cam sensor during a pull.  This would allow us to see the cam with the cam sensor on it advancing or retarding during the pull!

Back in 2006, on the second SOHC I ever built, I added proximity sensors and targets to the crank and both cams, and ran multiple experiments over a 4 week period trying to determine exactly how much the cams were moving with engine speed.  The datalogging capability I had back then was SLOW, and so I ran the pulls really slow, and tried to get data every 500 RPM or so.  It was quite the torture test for the engine, and gave me some surprising results.  What I found was that while the right cam retarded with RPM (as everybody always said they did), the left cam actually advanced with RPM.  This led to about a 3-4 degree variation in cam timing between the two cams, so ever since this I've been setting up my SOHC engines with the right cam advanced 3-4 degrees compared to the left cam.  The two graphs reprinted below summarize all this data:





The "calculated" vs. "measured" data in the second chart refers to calculating the difference between the two cam signals when they are compared to the crank signal, and then a directly measured difference between the two cams.  The data was taken on different days, so there are some minor differences, but the general trend is the same.  Now that we could see this same data logged directly from the EFI system, I was anxious to get some confirming data.

The cam sensor was on the left cam, so we were expecting it to advance.  After the next pull, the data seemed to show that the left cam was retarding, and by quite a significant amount!  However, there was some question about the data itself; could the direction be wrong?  We weren't sure, but in any case we were seeing something like 8 degrees of change in the cam phase.  Yikes!

While we were thinking about this, we decided to go ahead and put Scott's 8 O2 sensor setup on the engine.  Here's a picture of the engine with this setup installed:



This setup uses the closed loop corrections available in the MS3X to monitor the O2 sensors in each primary pipe, and then hold the injectors open a shorter or longer period of time, to try to hit the targeted A/F ratio in each cylinder.  After getting all the O2 sensors installed Scott configured the CAN communications in the software, and we were ready to run.  We targeted the A/F at 12.6:1, and ran the pull hoping for a significant power increase.  We did see a bump of about 10 HP, but it wasn't a real big improvement.  This basically meant that the sheet metal intake I had built for this engine, previously known as "the steaming pile" because of the problems it seemed to give us in 2011, was actually pretty good.  In fact, Scott was praising the steaming pile by the end of the day Sunday as one of the better sheet metal intakes he's seen with respect to fuel distribution. 

Last time I ran this engine on the dyno, in its 585" form, it had wanted to run a little lean.  So we ran another pull, changing the targeted A/F ratio to 13:1, and the engine really picked up, to the tune of about 18 HP.  That was good news.  We continued to log the cam data, and we continued to see what appeared to be a big retard in the left cam during the pull.  It was about the end of the night on Saturday, so we made plans for the next day and called it a night.

This morning (Sunday), the first thing I did when getting out to the shop was to take my second Hamlin sensor, and install it as an auxiliary cam sensor in the right valve cover.  I was certain that the right cam would retard with engine RPM, so if the right and left cams were moving in the same direction, we would have confirmation that both cams were retarding.  Thinking about this a little more, I began to suspect that the long, slow pulls I had done on the test engine back in 2006 were not really reflective of what would actually be happening at the track, and that maybe with the rapid logging available using the MS3X, and a normal dyno pull rate of 300 RPM/sec (rather than the 25 or 50 RPM/sec I was using in 2006) might make the cams behave differently.  When Scott arrived the first thing we did was run the test to look at the left and right cams together.  Sure enough, they were both moving in the same direction, and both retarding a significant amount.  Here are four screen shots from the MS3X datalogger that show this effect:



The vertical blue line running through the graph has numbers next to it, and these are the ones we want to pay attention to.  The top graph shows engine RPM, which is about 1200 at this point in the log.  The bottom graph shows the cam sensor angles.  These are phased arbitrarily, so what we are looking for is changes in these numbers, not absolute values.  The red line is the right cam sensor, and the white line is the left cam sensor.  At this point in the log the right cam is at 127.6 degrees, and the left cam is at 156.9 degrees.  Off to the right of the vertical blue line, you can see the engine RPM during the dyno pull.  Also, the left cam line goes vertical in the middle of the pull, but that's not real data, that is just a noise spike.  Here are the other graphs with the blue line positioned at various points during the pull:



In this graph we are at the start of the pull, 5000 RPM, and the right cam has retarded to 116.7 degrees, while the left cam has retarded to 153.7 degrees.  Here's the next graph:



Here we are at 6360 RPM, and the right cam has retarded to 115.3 degees, while the left cam has retarded to 149.7.  Here's the next graph:




In this case we are almost at the end of the pull, at 7180 RPM, and the right cam has retarded to 113.7 degrees, while the left cam has retarded to 147.0. 

To be honest I'm not really sure I believe these numbers; that is a tremendous amount of chain stretch, and it just seems unreasonable to me.  The difference between the right cam at idle (127.6 degrees) and the right cam at 5000 RPM (116.7 degrees) is just not believable.  Also, the left cam is retarding more during the pull (6.7 degrees) than the right cam (3.0 degrees).  This is in spite of the fact that as the engine spins the length of the chain between the drive sprocket and the left cam is shorter than the length of the chain between the drive sprocket and the right cam, in the direction of engine rotation.  If anything, the right cam should be retarding more than the left cam, if indeed they are both retarding as this data seems to suggest.  I can see several potential sources of error in this data, including variability in the targets (which are just bolt heads), and frequency response of the Hamlin sensors.  Just doing a quick calculation, at 7000 engine RPM the cams are spinning at 3500 RPM.  This is 58.33 rotations per second.  To discriminate 0.1 degrees of accuracy the update frequency of the sensors must be 1/(58.33 * 3600), or about 210 KHz, which is pretty fast for a magnetic sensor.  Even to discriminate 1.0 degrees the frequency response still has to be 21 KHz.  I need to do some research on the sensors to see if they are up to the drill here.

In any case more happened on Sunday than I have reported so far; I will update this post tomorrow with more information on Sunday's tests - Jay






207
The Road to Drag Week 2014 / The Road to Drag Week 2014 - June 15
« on: June 15, 2014, 08:18:43 PM »
Finally this week it felt like I got something accomplished on this project.  The last three weeks have been an unending string of fiddling around with minor issues, fabricating small parts, etc.  This process extended into this weekend, because I still had a few small fabrication projects to get finished.  These included making a bracket to bolt the fuel pressure regulator to the front timing cover, making four small L-shaped brackets to hold the EFI fuel rails in place (the old ones wouldn't work because my new injectors are taller, and position the fuel rail higher), making a fitting to install the vacuum relief valve for the dry sump system in the left valve cover, and making brackets to hold two short coolant lines from the intake manifold in place at the top of the front cover.  I was busy all week with other stuff, including Friday night, so I didn't get going on this until Saturday.  It took me until 11:00 PM Saturday night to get all this finished up, plus make up the coolant and fuel lines!  It just didn't seem like it would be that much work, but it took forever.

Finally, though, all that was behind me at the end of the night on Saturday.  Before turning in I decided to bolt on my new engine sling.  One of the issues with these engines when you use the Hilborn setup or this sheet metal intake is that it is difficult to find a place to bolt the engine lift chains on, where they won't be pushing against some fragile tube or other sensitive part of the engine when you lift it up.  A while back I stumbled across this new engine sling that uses nylon straps to bolt to the exhaust ports, and just lifts the engine by those straps.  The straps rest against the valve cover as they come up to the top of the engine, which of course isn't a real fragile part.  I figured this thing would be perfect for lifting up the SOHC, so I picked one up.  Here's a photo of the engine ready to come off the stand, with the new sling bolted on:



Sunday morning I got to work taking the 428CJ off the dyno, where it has been sitting ever since I ran the intake adapter dyno tests.  By noon I had the engine off and the dyno room cleaned up and ready to take the SOHC.  After rolling the SOHC into the dyno room and attaching the flywheel, bellhousing, engine mounts, etc., I got the engine up in the air and ready to bolt on the dyno.  It was at this moment that I discovered a limitation of my new engine sling  ::)  You can't really tell in the picture below, but the attachment point for the lift crane is so high up over the engine that I didn't have enough height to get the engine high enough to mount on the dyno, without having the crane hit the ceiling:



I ended up getting it up in the air as high as I could, and then putting a small jack under the back of the engine to raise it so that the dyno's drive shaft could slide into the bellhousing and engage the drive hub bolted to the flywheel.  Nothing is ever easy with this stuff.  Anyway, by 2:00 I had the engine bolted down on the dyno stand.  Next I had to figure out a way to mount the dry sump tank in approximately the same relative location as it would be in the car, and then make all the dry sump lines.  While I was at it I installed the headers, to make sure that I had clearance to all the dry sump components.  Finally when all that was done I filled the oil filter and dry sump tank with 7 quarts of oil, took the pump loose so I could remove the belt, and spun the dry sump pump to pre-oil the engine.  Everything went according to plan, and I got good oil pressure during the pre-oil.  Here are a couple of photos of the engine on the dyno, and also one close up of the dry sump components that are chassis mounted:







I still have a lot to do to get this engine running, including hooking up the exhaust, cooling system, and fuel system, plus all the wiring and programming the EFI software, but I think that's all do-able this week, so I should be running on the dyno by the end of next weekend.  I'll post another update next Sunday night.



208
Member Projects / FE Timing Cover
« on: June 10, 2014, 08:08:52 PM »
I regularly find myself bemoaning the fact that I always seem to be behind schedule on my various projects.  Many of my friends, and my wife, always point out that I am trying to do too much all at once.  I have no doubt that this is true; perhaps it is a feature of my personality that I'm not happy without several balls in the air at once, so to speak.

Here is the latest "ball in the air".  Knowing full well I would get my share of flack from machoneman (LOL!), I embarked on another project reminiscent of the old products from Pro-Stock Engineering.  I had always admired their timing cover, with the removable plate allowing access to the top cam gear.  I thought the basic idea was great, but that it needed a few more features to really take it to the limit.  So, several months ago I started drawing up the FE Power timing cover.  I did this in 2D CAD, and then the pattern maker that I have been working with on the intake adapters turned it into a 3D model.  Here are a couple of screen shots of the machined model:





Let me point out some of the features of this timing cover.  First, of course, there is the large opening allowing access to the top cam gear and the cam.  The cover for this is going to be a laser cut steel plate.  Notice the groove around the large opening; this is for an O-ring seal, so that no gasket will be required to seal the opening.  I chose a steel plate for the cover to make sure it was rigid enough to compress the O-ring evenly between the attachment bolts, for a good seal.  I will provide button head cap screws to bolt on the plate, and powder coat it for a nice appearance.

You will also notice five extra bosses on this cover, around the opening for the crankshaft.  These will be drilled and tapped as blind holes, for use in attaching brackets to the timing cover.  With my experiences in EFI I think it would be very helpful to be able to attach a bracket for a crank sensor directly to the top surface of the timing cover.  In addition, with most electric water pumps available these days there is no provision for mounting brackets to hold the alternator or other accessories (my CVR water pump adapters being the exception).  Especially for a low mount alternator, I thought that bosses like this would be very useful for use as a starting point for brackets if an electric water pump was used.  Also, on the back side of the cover these bosses have some strengthening ribs; they may even be strong enough to use as a motor plate mount, although I'm really not sure about that at this point.

Also, there is a raised area around the crankshaft opening on the front of the cover.  This is there so that a front seal can be installed in this position.  Now, the back side of the cover also has the standard position for the front seal.  The idea here is that you can use two seals, one reversed, and be able to seal the engine either with a vacuum pump/dry sump, or if the engine is running normally with some pressure in the crankcase.  I've often run vacuum pumps on my engines, and usually I run with them disconnected on the street, so that you need the regular front seal.  But when you connect them at the track, you need the reverse seal for optimum sealing.  With the two seals, your engine is sealed up either way.  One question about this approach, by the way, is will the front seal survive if the back seal is working effectively; in other words, if the front seal is not exposed to oil, will it eventually burn up?  I was talking to Blair Patrick about this a while back when I was doing the design, and he suggested putting a little grease between the two seals, so I'm going to try that and see if both seals will live.  If they don't, well I can just machine off the boss for the seal on the front of the cover.  One other idea with this is to just use the seal in the normal location, and if the seal goes out, you can install one in the front more easily than replacing the one in the normal position.

I don't know how many people have had problems stripping the corner oil pan attachment bolts out of the factory front covers, but I certainly have, so I made this area of my cover thicker to allow more thread distance.  Also the bottom front bolts are extended out with a boss, so that the head of the bottom bolt doesn't interfere with a longer oil pan bolt in the corner. 

On the laser cut steel cover there will be two small threaded holes for attaching a factory timing pointer.  One downside to this arrangement is that you will have to remember to put some sealer on the threads of those bolts, in order to prevent an oil leak there.  And one other thing about that steel cover is that it can easily be drilled for a 1/2" barrel cam sensor, and a simple target like a bolt put into the top cam gear to make the cam sensor functional.  Again this is an easy way to run a cam sensor in a full sequential EFI application, without having to buy a special distributor.

Several weeks ago I pulled the trigger on the casting patterns for this design.  They were done in mid-May, and today I picked up the first prototype castings.  Here's a few pictures:









The squared-off part at the top of the opening is there for initial fixturing purposes only, and will be machined off as shown in the CAD model during the machining operations.  I was ready to get started with the machining programs a couple of weeks ago but I am still behind on getting some of the intake adapter machining programs finished (such as the one for CHI ports in my standard intake adapter, and the standard version of the high riser adapter), so I was a little conflicted about starting this project.  As it turned out, though, the pattern maker has some free time on his CNC machines, and he was able to quote me a very competitive price for machining these things.  So, on the castings themselves I won't have to machine them myself at all, at least at first; the pattern guys are going to make all the fixtures so that they will work on my machine or on theirs, and are willing to machine the first 100 castings.  That frees me up to keep going on the intake adapters.  I will have to do some very minor machine work on the steel cover plates, and also powder coat them, but this won't require a significant time investment.

For this particular product I'm going to use the same rationale that I used for the FE intake adapters, which is to try to sell 100 covers and amortize my tooling costs over those covers.  I think I should be able to sell 100 of them, but we will see.  They'll be priced at around $225 complete.  After I get the first prototypes machined, hopefully within the next month or so, I will test one out on one of my dyno mules, and if everything looks good, I'll post an ad in the vendor classifieds and start a list of people who want one. 

So, what do you guys think?  Will this be a worthwhile product?

209
The Road to Drag Week 2014 / The Road to Drag Week 2014 - June 8
« on: June 09, 2014, 12:11:51 AM »
It's been another week of slow going on this project, and I am now officially behind schedule (imagine that LOL!).  Seems like all I've been doing for the last 3 weeks is fabrication work.  After pulling out the sheet metal intake last week I realized I needed to make some changes, and this included some welding and grinding on the intake, plus programming and machining a 1/2" delrin spacer.  And then some kind of a stomach bug hit me today and I hardly got anything done.  But on Saturday night before I got sick I did finish up the work on the intake manifold and the spacer, and got it mounted on the engine.  I also stuck on the headers to help me figure out where all the dry sump lines would have to run, and installed the fuel rails and injectors so I had an idea what I would have to do about the fuel system.  I just got off the Summit Racing site, ordering all the plumbing that I need to finish this up.  Basically, with the intake manifold finished, I'm down to making up a few new brackets and some lines, plus the throttle linkage, and then this engine can finally go on the dyno.  Next weekend I'll have it on the dyno for sure, although probably not running because I still need to do all the wiring work.  But I'm getting closer.  Here's a picture of the engine as it sits tonight on the stand:



I should have more details to share next weekend...

210
The Road to Drag Week 2014 / The Road to Drag Week 2014 - June 2
« on: June 02, 2014, 08:13:29 PM »
I have to chalk this week up as another frustrating one, where I spent a pretty fair amount of time working on this project but really didn't get a lot accomplished.  Over the weekend I spent way more time than I expected doing more machining for the front mounted parts of the engine.  My dry sump gear arbor needed to be shortened, and the little bracket that holds the crank sensor seemed to take forever to machine.  Plus I had forgotten that I had used some washers to space out the alternator pulley that goes on the crank, so I had to machine a donut to replace those.  Pretty much took me all day Saturday, and Sunday morning to get all that done.  Here are a couple of pictures of the crank sensor bracket, and how it looks mounted on the engine:







Next I made up the dry sump oil lines that go to the pan; here's a picture of those:



After that was done I was FINALLY able to flip the engine right side up again, and start thinking about installing the intake manifold.  Of course, pulling it off the shelf it was pretty dirty, and so I had to pull it all apart and get it cleaned up before I could put it on the engine.  Here's a picture of the lower part of the intake, just sitting in place:



Here's a shot down one of the runners:



Pretty straight shot to the valve, that's for sure.  As I was inspecting this whole thing I realized that there were going to be some modifications that I wanted to make to this manifold, based on what I've learned about sheet metal intakes since I built this one back in 2010.  By the way, any suggestions from you guys on how much plenum volume I should use for this manifold?  I'm following the rule of thumb that you should have one cubic inch of plenum volume for each cubic inch of engine displacement on a sheet metal intake like this, but one of the modifications I'm planning is some spacer plates that go between the plenum top and the intake base, to increase plenum volume if necessary.  To me, just looking at it, the plenum appears too small, or at least the top of the plenum box is too close to the top of the runners, but I really don't know for sure.  One thing I do know is that the runner lengths are off based on my intended RPM range, which is up to a redline of 7500 RPM.  But at this point there's not too much I can do about that, and in fact even if I started a new manifold from scratch it would be difficult to get runners that were 1.5" or 2.0" longer without tipping them way up, so that the air would have to bend going into the port.  At the time I built the manifold I didn't want to do that, so I'm living with a less than ideal runner length to keep a straight shot at the port.  Here's a couple of pictures of the manifold top in place:





Those throttle bodies are rated at 1170 cfm each; just like two Dominators!  Coming in from the front makes the tall induction system work with my hood scoop, but I'm sure that I'm leaving power on the table without having the normal Dominator carbs or throttle bodies on top of the plenum.  I'm hoping this doesn't cost me too much power.  I guess we'll see on the dyno.

I should be able to get the modifications I want made to the intake this week, so that hopefully this engine will finally get mounted on the dyno next weekend.  Then I've got a bunch of wiring in front of me before I can run it.  It's June already, and Drag Week is only 3 months away!  I need to get this engine running...

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